To improve the vibration-isolation performance of cab seats,the optimization model of the seat suspension system of construction machinery cabs is proposed based on the negative stiffness structure.The negative stiffn...To improve the vibration-isolation performance of cab seats,the optimization model of the seat suspension system of construction machinery cabs is proposed based on the negative stiffness structure.The negative stiffness nonlinear kinetic equation is established by designing the seat negative stiffness suspension structure(NSS).Using MATLAB,the different parameters of the suspension system and their influences on the dynamic stiffness are analyzed.The ideal configuration parameter range of the suspension system is obtained.Meanwhile,the optimization model of NSS is proposed,and the vibration transmissibility characteristics are simulated and analyzed by different methods.The results show that the displacement and acceleration amplitudes of the optimized seat suspension system are evidently reduced,and the four-time power vibration dose value and root mean square calculation values in the vertical vibration direction of the seat decrease by 86%and 87%,respectively.Seat effective amplitude transmissibility(SEAT)and the vibration transmissibility ratio values also decrease.Moreover,the peak frequencies of the vibration transmitted to the driver deviate from the key frequency values,which easily cause human discomfort.Thus,the design of the seat suspension system has no effect on the health condition of the driver after being vibrated.The findings also illustrate that the NSS suspension system has good vibration-isolation performance,and the driver's ride comfort is improved.展开更多
To improve the driving comfort of combine harvesters,driver seat low-frequency vibration and related driver ride-comfort problems were investigated on a Chinese CFFL-850 crawler-type full-feed combine harvester based ...To improve the driving comfort of combine harvesters,driver seat low-frequency vibration and related driver ride-comfort problems were investigated on a Chinese CFFL-850 crawler-type full-feed combine harvester based on ISO2631.Driver vibration and driving seat transmission characteristics were measured under the following conditions:no-load idling,driving on the road,driving in the field,and simulated harvesting.The root mean square values composite vibration under four conditions were 3.63 m/s^(2),2.35 m/s^(2),3.34 m/s^(2),and 2.67 m/s^(2),respectively.For the same condition,the maximum root mean square scores of vibration component on driver whole-body occurred in the seat support surface(test point 1)and vertical direction(Z direction),which were 3.56 m/s^(2),2.05 m/s^(2),3.15 m/s^(2),and 2.43 m/s^(2),respectively.The test point 2 to test point 1 vertical-transfer function curve trends were nearly identical.Nearly all of the transfer coefficients were greater than 1 in the range of 1-50 Hz,therefore,the seat vibration attenuation performance was poor.Based on the analysis results,the driver seat structure was altered and a verification test was performed.The test results indicated that after an X-damping mechanism was installed,vibration acceleration,on the surface of the seat support under the road-driving conditions,decreased from 2.35 m/s^(2) to 1.68 m/s^(2).Under the simulated harvesting condition,the vibration acceleration decreased from 2.56 m/s^(2) to 1.46 m/s^(2).Nearly all of the seat vertical transfer coefficients were less than 1 within the frequency range of 1-80 Hz,therefore the dynamic comfort of the seat was ameliorated after structural improvement.展开更多
基金The National Natural Science Foundation of China(No.11902207,No.52072072)the Natural Science Foundation of Hebei Province(A2020210018)Higher Education Teaching Research Project(No.Y2020-15).
文摘To improve the vibration-isolation performance of cab seats,the optimization model of the seat suspension system of construction machinery cabs is proposed based on the negative stiffness structure.The negative stiffness nonlinear kinetic equation is established by designing the seat negative stiffness suspension structure(NSS).Using MATLAB,the different parameters of the suspension system and their influences on the dynamic stiffness are analyzed.The ideal configuration parameter range of the suspension system is obtained.Meanwhile,the optimization model of NSS is proposed,and the vibration transmissibility characteristics are simulated and analyzed by different methods.The results show that the displacement and acceleration amplitudes of the optimized seat suspension system are evidently reduced,and the four-time power vibration dose value and root mean square calculation values in the vertical vibration direction of the seat decrease by 86%and 87%,respectively.Seat effective amplitude transmissibility(SEAT)and the vibration transmissibility ratio values also decrease.Moreover,the peak frequencies of the vibration transmitted to the driver deviate from the key frequency values,which easily cause human discomfort.Thus,the design of the seat suspension system has no effect on the health condition of the driver after being vibrated.The findings also illustrate that the NSS suspension system has good vibration-isolation performance,and the driver's ride comfort is improved.
基金This research was supported by the National Natural Science Foundation of China(51475217)the Fok Ying-Tong Education Foundation of China(Grant No.141051)+1 种基金Six Talent Peaks Project in Jiangsu Province(NY-024)a project funded by the Priority Academic Program Development(PAPD)of Jiangsu Higher Education Institutions.
文摘To improve the driving comfort of combine harvesters,driver seat low-frequency vibration and related driver ride-comfort problems were investigated on a Chinese CFFL-850 crawler-type full-feed combine harvester based on ISO2631.Driver vibration and driving seat transmission characteristics were measured under the following conditions:no-load idling,driving on the road,driving in the field,and simulated harvesting.The root mean square values composite vibration under four conditions were 3.63 m/s^(2),2.35 m/s^(2),3.34 m/s^(2),and 2.67 m/s^(2),respectively.For the same condition,the maximum root mean square scores of vibration component on driver whole-body occurred in the seat support surface(test point 1)and vertical direction(Z direction),which were 3.56 m/s^(2),2.05 m/s^(2),3.15 m/s^(2),and 2.43 m/s^(2),respectively.The test point 2 to test point 1 vertical-transfer function curve trends were nearly identical.Nearly all of the transfer coefficients were greater than 1 in the range of 1-50 Hz,therefore,the seat vibration attenuation performance was poor.Based on the analysis results,the driver seat structure was altered and a verification test was performed.The test results indicated that after an X-damping mechanism was installed,vibration acceleration,on the surface of the seat support under the road-driving conditions,decreased from 2.35 m/s^(2) to 1.68 m/s^(2).Under the simulated harvesting condition,the vibration acceleration decreased from 2.56 m/s^(2) to 1.46 m/s^(2).Nearly all of the seat vertical transfer coefficients were less than 1 within the frequency range of 1-80 Hz,therefore the dynamic comfort of the seat was ameliorated after structural improvement.