In Shougang Jingtang 5 500m 3 huge blast furnace ( BF ) design , dome combustion hot blast stove ( DCHBS ) technology is developed.DCHBS process is optimized and integrated , and reasonable hot blast stove ( HBS ) tec...In Shougang Jingtang 5 500m 3 huge blast furnace ( BF ) design , dome combustion hot blast stove ( DCHBS ) technology is developed.DCHBS process is optimized and integrated , and reasonable hot blast stove ( HBS ) technical parameters are determined.Mathematic model is established and adopted by computational fluid dynamics ( CFD ) .The transmission theory is studied for hot blast stove combustion and gas flow , and distribution results of HBS velocity field , CO density field and temperature field are achieved.Physical test model and hot trail unit are established , and the numeral calculation result is verified through test and investigation.3-D simulation design is adopted.HBS process flow and process layout are optimized and designed.Combustion air two-stage high temperature preheating technology is designed and developed.Two sets of small size DCHBSs are adopted to preheat the combustion air to 520-600℃.With the precondition of BF gas combustion , the hot blast stove dome temperature can exceed 1 420 ℃. According to DCHBS technical features , reasonable refractory structure is designed.Effective technical measures are adopted to prevent hot blast stove shell intercrystalline stress corrosion.Hot blast stove hot pipe and lining system are optimized and designed.After blowing in , the blast temperature keeps increasing , and the monthly average blast temperature reaches 1 300℃ when burning single BF gas.展开更多
A high blast temperature is an effective measure that improves pulverized coal injection (PCI)and energy consumption,decreases the cost of blast furnaces (BF). Apart from using technology such as the increased vau...A high blast temperature is an effective measure that improves pulverized coal injection (PCI)and energy consumption,decreases the cost of blast furnaces (BF). Apart from using technology such as the increased vault temperature of the hot-blast stove, the increased temperature of the waste gas, the preheating of combustion air and gas, and fully closed mixed air valves, other measures, such as using an oxygen-enriched blast stove, burning high heating value converter gas, increasing the number of stove changes to reduce the time needed for stove blasts, were taken to increase the blast temperature of the 2 500 m3 BF in recent years. The blast temperature of the 2 500 m3 BF was continuously increased in these years. The monthly average temperature of the 2 500 m3 BF reached 1 158℃, with the highest blast temperature reaching 1 195 ℃ in 2006. This technique of increased blast temperatures has reached an advanced level in China.展开更多
The shrinkage behavior of high performance cement concrete made from Portland cement, ultra fine granulated blast furnace slag and pulverized fly ash with addition of superplasticizer at different temperatures from am...The shrinkage behavior of high performance cement concrete made from Portland cement, ultra fine granulated blast furnace slag and pulverized fly ash with addition of superplasticizer at different temperatures from ambient temperature to 120 ℃ under different seuliug conditions was investigated by means of length change measurement on cylindrical concrete specimens along with curing age. Results show that drying shrinkage deformations of titled concrete specimens increased rapidly as the curing temperature rose. The development of dryiing shrinkage deformatian can be efficiently controlled with the aid of aluminum tape sealing as compared with the unsealed specimens, especially when the curing temperature is below 60℃ , although it will increase dramatically when the curing temperature is elevated to above 90%" . Polymer coating on concrete specimens showed a similar effect on the control of drying shrinkage as the sealing operation with aluminum tape.展开更多
文摘In Shougang Jingtang 5 500m 3 huge blast furnace ( BF ) design , dome combustion hot blast stove ( DCHBS ) technology is developed.DCHBS process is optimized and integrated , and reasonable hot blast stove ( HBS ) technical parameters are determined.Mathematic model is established and adopted by computational fluid dynamics ( CFD ) .The transmission theory is studied for hot blast stove combustion and gas flow , and distribution results of HBS velocity field , CO density field and temperature field are achieved.Physical test model and hot trail unit are established , and the numeral calculation result is verified through test and investigation.3-D simulation design is adopted.HBS process flow and process layout are optimized and designed.Combustion air two-stage high temperature preheating technology is designed and developed.Two sets of small size DCHBSs are adopted to preheat the combustion air to 520-600℃.With the precondition of BF gas combustion , the hot blast stove dome temperature can exceed 1 420 ℃. According to DCHBS technical features , reasonable refractory structure is designed.Effective technical measures are adopted to prevent hot blast stove shell intercrystalline stress corrosion.Hot blast stove hot pipe and lining system are optimized and designed.After blowing in , the blast temperature keeps increasing , and the monthly average blast temperature reaches 1 300℃ when burning single BF gas.
文摘A high blast temperature is an effective measure that improves pulverized coal injection (PCI)and energy consumption,decreases the cost of blast furnaces (BF). Apart from using technology such as the increased vault temperature of the hot-blast stove, the increased temperature of the waste gas, the preheating of combustion air and gas, and fully closed mixed air valves, other measures, such as using an oxygen-enriched blast stove, burning high heating value converter gas, increasing the number of stove changes to reduce the time needed for stove blasts, were taken to increase the blast temperature of the 2 500 m3 BF in recent years. The blast temperature of the 2 500 m3 BF was continuously increased in these years. The monthly average temperature of the 2 500 m3 BF reached 1 158℃, with the highest blast temperature reaching 1 195 ℃ in 2006. This technique of increased blast temperatures has reached an advanced level in China.
文摘The shrinkage behavior of high performance cement concrete made from Portland cement, ultra fine granulated blast furnace slag and pulverized fly ash with addition of superplasticizer at different temperatures from ambient temperature to 120 ℃ under different seuliug conditions was investigated by means of length change measurement on cylindrical concrete specimens along with curing age. Results show that drying shrinkage deformations of titled concrete specimens increased rapidly as the curing temperature rose. The development of dryiing shrinkage deformatian can be efficiently controlled with the aid of aluminum tape sealing as compared with the unsealed specimens, especially when the curing temperature is below 60℃ , although it will increase dramatically when the curing temperature is elevated to above 90%" . Polymer coating on concrete specimens showed a similar effect on the control of drying shrinkage as the sealing operation with aluminum tape.