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A Novel Close-loop Strategy for Integrating Process Operations of Fluidized Catalytic Cracking Unit with Production Planning Optimization 被引量:4
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作者 王如强 李初福 +1 位作者 何小荣 陈丙珍 《Chinese Journal of Chemical Engineering》 SCIE EI CAS CSCD 2008年第6期909-915,共7页
Production planning models generated by common modeling systems do not involve constraints for process operations, and a solution optimized by these models is called a quasi-optimal plan. The quasi-optimal plan cannot... Production planning models generated by common modeling systems do not involve constraints for process operations, and a solution optimized by these models is called a quasi-optimal plan. The quasi-optimal plan cannot be executed in practice some time for no corresponding operating conditions. In order to determine a practi- cally feasible optimal plan and corresponding operating conditions of fluidized catalytic cracking unit (FCCU), a novel close-loop integrated strategy, including determination of a quasi-optimal plan, search of operating conditions of FCCU and revision of the production planning model, was proposed in this article. In the strategy, a generalized genetic algorithm (GA) coupled with a sequential process simulator of FCCU was applied to search operating conditions implementing the quasi-optimal plan of FCCU and output the optimal individual in the GA search as a final genetic individual. When no corresponding operating conditions were found, the final genetic individual based correction (FGIC) method was presented to revise the production planning model, and then a new quasi-optimal production plan was determined. The above steps were repeated until a practically feasible optimal plan and corresponding operating conditions of FCCU were obtained. The close-loop integrated strategy was validated by two cases, and it was indicated that the strategy was efficient in determining a practically executed optimal plan and corresponding operating conditions of FCCU. 展开更多
关键词 production planning process operations fluidized catalytic cracking unit integrated strategy
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Decoupling Control of Fluid Catalytic Cracking Unit 被引量:1
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作者 Duraid Fadhil Ahmed 《Journal of Chemistry and Chemical Engineering》 2011年第1期12-19,共8页
This study presents a decoupling control scheme of fluid catalytic cracking unit to account for the high interaction between two temperature control loops. The feed flow rate load disturbance is introduced to test the... This study presents a decoupling control scheme of fluid catalytic cracking unit to account for the high interaction between two temperature control loops. The feed flow rate load disturbance is introduced to test the proposed decoupling control scheme. Through simulation study shown that the decoupling is effective, stable and it presents advantage over controller without decoupler. Also, this scheme is able to offer good dynamic performance for most disturbances. 展开更多
关键词 Control of fluid catalytic cracking unit multivariable control decoupling control.
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Failure analysis of corrosion cracking and simulated testing for a fluid catalytic cracking unit
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作者 HuaChen XiaogangLi +2 位作者 ChaofangDong MingLi JinwenYang 《Journal of University of Science and Technology Beijing》 CSCD 2005年第2期172-177,共6页
The failure of a fluid catalysis and cracking unit (FCCU) in a Chinese refinery was investigated by using nondestructive detection methods, fracture surface examination, hardness measurement, chemical composition and... The failure of a fluid catalysis and cracking unit (FCCU) in a Chinese refinery was investigated by using nondestructive detection methods, fracture surface examination, hardness measurement, chemical composition and corrosion products analysis. The results showed that the failure was caused by the dew point nitrate stress corrosion cracking. For a long operation period, the wall temperature of the regenerator in the FCCU was below the fume dew point. As a result, an acid fume NOx-SOx-H2O medium present- ed on the surface, resulting in stress corrosion cracking of the component with high residual stress. In order to confirm the relative conclusion, simulated testing was conducted in laboratory, and the results showed similar cracking characteristics. Finally, some sug- gestions have been made to prevent the stress corrosion cracking of an FCCU from re-occurring in the future. 展开更多
关键词 stress corrosion cracking fluid catalytic cracking unit dew point FAILURE
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7-lump kinetic model for residual oil catalytic cracking 被引量:2
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作者 XU Ou-guan SU Hong-ye +1 位作者 MU Sheng-jing CHU Jian 《Journal of Zhejiang University-Science A(Applied Physics & Engineering)》 SCIE EI CAS CSCD 2006年第11期1932-1941,共10页
In this paper a novel 7-lump kinetic model is proposed to describe residual oil catalytic cracking, in which coke is lumped separately for accurate prediction. The reactor block is modeled as a combination of an ideal... In this paper a novel 7-lump kinetic model is proposed to describe residual oil catalytic cracking, in which coke is lumped separately for accurate prediction. The reactor block is modeled as a combination of an ideal pipe flow reactor (PFR) and a continuously stirred tank reactor (CSTR). Unit factors are designed to correct the deviation between model predictions and practical plant data and tuned by modified Levenberg-Marquardt algorithm. The parameters estimated are reliable and good agreement between the model predictions and plant observations is observed. The model helps us get good insight into the per- formance of an industrial riser reactor that would be useful for optimization of residual oil catalytic cracking. 展开更多
关键词 Residua catalytic cracking (RCC) 7-lump kinetic model unit factor
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Study and Strategy on Expansion of Steam Cracking Unit to 650 kt/a at Yanshan Petrochemical Company
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作者 Cao Xianghong (SINOPEC, Beijing 100011) 《工程科学(英文版)》 2003年第2期1-12,共12页
After having expanded its capacity from 300 kt/a to 450 kt/a in 1994, the steam cracking unit of Yanshan Petrochemical Company was still experiencing such problems as low feedstock flexibility, high energy consumption... After having expanded its capacity from 300 kt/a to 450 kt/a in 1994, the steam cracking unit of Yanshan Petrochemical Company was still experiencing such problems as low feedstock flexibility, high energy consumption and smaller production capacity as compared to other ethylene units constructed in the same time. In order to fully improve technical capability, reduce energy consumption, improve feedstock flexibility and increase production capacity of steam crackers, a lot of technical transform schemes on steam cracking were studied and compared with attention focused on the feasibility, safety, operability of the related revamp schemes, as well as the advanced nature and economical features. The transform scheme decided includes following projects. For the pyrolysis quench compression system, the pyrolysis gasoline fractionation tower is retrofitted on the site, quench water tower, pyrolysis gas compressor and steam turbine are replaced by new ones respectively. For the separation system a low pressure methane removal technology is adopted with the demethanizer tower replaced, coupled with the C 3 catalytic rectification/hydrogenation technology, while the high pressure depropanizer is replaced with addition of a propylene rectification tower. The fractionation flow sheet and equipment are adjusted with addition of a propylene compressor and compressor for binary mixture of methane ethylene cooling agents. The revamped complex has expanded the ethylene capacity to the target of 660 kt/a with the actual capacity reaching 710 kt/a, remarkably reduced the energy consumption, and is capable of using naphtha, light diesel fuel, heavy diesel fuel and the hydrocracked tail oil as the steam cracking feedstock. This project is the first to apply refrigeration by means of a mixed cooling agent and has succeeded in using C\-3 catalytic rectification/hydrogenation technology, which has given an impetus to the progress of steam cracking industry in the world. 展开更多
关键词 EXPANSION steam cracking unit binary mixed cooling agent catalytic RECTIFICATION HYDROGENATION technology
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紧急停车系统在FCCU反应再生过程中的应用 被引量:1
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作者 李鸣 梁英 《自动化仪表》 CAS 北大核心 2011年第8期43-46,共4页
反应再生过程的安全运行是整个催化裂化装置安全生产的必要前提。为最大限度地降低装置恶性事故发生的概率,避免重大经济损失,在深入了解其工艺及设备特点的基础上,研究并设计了一套基于西门子S7-300 PLC的紧急停车(ESD)系统。介绍了ES... 反应再生过程的安全运行是整个催化裂化装置安全生产的必要前提。为最大限度地降低装置恶性事故发生的概率,避免重大经济损失,在深入了解其工艺及设备特点的基础上,研究并设计了一套基于西门子S7-300 PLC的紧急停车(ESD)系统。介绍了ESD的联锁控制、硬件配置、软件组态和网络通信等。该系统可对装置进行进料自保、两器自保、主风低流量自保以及主风机组自保,具有一定的工程意义。 展开更多
关键词 催化裂化装置 反应再生 S7-300PLC 紧急停车 连锁控制 组态
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Study on Commercial Application of FP-DSN Sulfur Transfer Additive in FCC Unit 被引量:2
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作者 Gao Siming Han Rongxian Chen Desheng(SINOPEC Qingdao Petrochemical Company,Qingdao 266043) 《China Petroleum Processing & Petrochemical Technology》 SCIE CAS 2009年第2期15-19,共5页
The FCC unit with addition of various inventories of the FP-DSN type sulfur transfer additive was tested in a commercial scale. The effect of the sulfur transfer additive was analyzed by investigating the indicators r... The FCC unit with addition of various inventories of the FP-DSN type sulfur transfer additive was tested in a commercial scale. The effect of the sulfur transfer additive was analyzed by investigating the indicators related with the regenerator flue gas composition,the dry gas composition before desulfurization,the LPG composition before desulfurization,the acid gas,and the yield of gasoline and diesel. The test results indicated that the sulfur was trans ferred from the feed stream into the dry gas,LPG and acid gas,and the sulfur transfer effect was obvious only when the inventory of sulfur transfer additive exceeded over 2.0% of total FCC catalyst inventory. 展开更多
关键词 catalytic cracking unit sulfur transfer additive commercial application
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Modeling and optimum operating conditions for FCCU using artificial neural network 被引量:6
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作者 李全善 李大字 曹柳林 《Journal of Central South University》 SCIE EI CAS CSCD 2015年第4期1342-1349,共8页
A self-organizing radial basis function(RBF) neural network(SODM-RBFNN) was presented for predicting the production yields and operating optimization. Gradient descent algorithm was used to optimize the widths of RBF ... A self-organizing radial basis function(RBF) neural network(SODM-RBFNN) was presented for predicting the production yields and operating optimization. Gradient descent algorithm was used to optimize the widths of RBF neural network with the initial parameters obtained by k-means learning method. During the iteration procedure of the algorithm, the centers of the neural network were optimized by using the gradient method with these optimized width values. The computational efficiency was maintained by using the multi-threading technique. SODM-RBFNN consists of two RBF neural network models: one is a running model used to predict the product yields of fluid catalytic cracking unit(FCCU) and optimize its operating parameters; the other is a learning model applied to construct or correct a RBF neural network. The running model can be updated by the learning model according to an accuracy criterion. The simulation results of a five-lump kinetic model exhibit its accuracy and generalization capabilities, and practical application in FCCU illustrates its effectiveness. 展开更多
关键词 radial basis function(RBF) neural network self-organizing gradient descent double-model fluid catalytic cracking unit(Fccu
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新型余热锅炉在RFCCU上的应用
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作者 丁泉 董国森 《黑龙江石油化工》 2000年第4期14-16,20,共4页
锦州石化公司投产的1.4 M t/a重油催化裂化装置的烟气余热锅炉成功应用了美国德尔塔公司锅炉技术,与国内设计比较具有结构简单、布置紧凑、工艺技术先进等优点.
关键词 余热锅炉 重油 催化裂化装置 积木式结构
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FCC再生烟气氮氧化物产生原因与控制措施 被引量:1
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作者 宋亦伟 赵勇 +1 位作者 徐猛 葛晓君 《辽宁化工》 CAS 2024年第2期326-328,共3页
介绍了青岛石油化工有限责任公司1.4 Mt·a^(-1)两段再生工艺重油催化裂化装置,分析了造成再生混合烟气中氮氧化物含量上升的原因,通过对再生系统优化操作、加注脱硝剂,使混合烟气中氮氧化物质量浓度由380 mg·m^(-3)降至150 mg... 介绍了青岛石油化工有限责任公司1.4 Mt·a^(-1)两段再生工艺重油催化裂化装置,分析了造成再生混合烟气中氮氧化物含量上升的原因,通过对再生系统优化操作、加注脱硝剂,使混合烟气中氮氧化物质量浓度由380 mg·m^(-3)降至150 mg·m^(-3),减轻了下游脱硝装置运行的苛刻度,实现了烟气的达标排放。 展开更多
关键词 催化裂化装置 再生烟气 氮氧化物 脱硝剂
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催化裂化装置液化石油气进料泵振动超标工艺处置和优化改造
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作者 王瑞 徐凯勃 +2 位作者 王为民 安宏利 程道建 《石油化工设备》 CAS 2024年第6期69-73,共5页
中国石油四川石化有限责任公司250万t/a催化裂化装置产品精制单元的液化石油气(简称液化气)进料泵频繁出现振动超标后干气密封泄漏故障,导致装置生产波动或非计划停工。分析了液化气进料泵故障产生原因。针对液化气进料泵振动超标后阀... 中国石油四川石化有限责任公司250万t/a催化裂化装置产品精制单元的液化石油气(简称液化气)进料泵频繁出现振动超标后干气密封泄漏故障,导致装置生产波动或非计划停工。分析了液化气进料泵故障产生原因。针对液化气进料泵振动超标后阀门内漏导致的无法切换隔离问题,创新使用了扩大流程法,实现了液化气进料泵的安全有效切换隔离。采用调整额定体积流量、更换泵型号、更换电机和机械密封等方法对液化气进料泵进行了技术改造优化,使液化气进料泵振动值从7~10 mm/s大幅降至2.1 mm/s以下,对催化裂化装置长周期安全平稳运行起到了积极作用。 展开更多
关键词 液化石油气进料泵 催化裂化装置 振动 密封 改造
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催化裂解装置液化石油气分离系统脱丙烷方案优化 被引量:1
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作者 李春晓 《炼油技术与工程》 CAS 2024年第7期1-4,共4页
随着催化裂解装置裂解深度的增加,液化石油气中二烯烃含量增加。液化石油气分离常规流程中脱丙烷塔底温度约108℃,较高的温度增加了二烯烃聚合的可能性,影响装置运行周期和经济效益,国内几家催化裂解液化石油气分离装置的脱丙烷塔普遍... 随着催化裂解装置裂解深度的增加,液化石油气中二烯烃含量增加。液化石油气分离常规流程中脱丙烷塔底温度约108℃,较高的温度增加了二烯烃聚合的可能性,影响装置运行周期和经济效益,国内几家催化裂解液化石油气分离装置的脱丙烷塔普遍存在塔釜和重沸器结焦堵塞的情况。在实际生产中为了缓解脱丙烷塔底结焦引起的停工等问题,通常在进料和塔底物料中加入阻聚剂,以降低物料聚合速率。文中分析了压力对脱丙烷体系相对挥发度和塔底温度的影响,得出较低的塔压有利于降低塔釜温度、提高轻重关键组分的相对挥发度,使分离更容易。塔压在0.9~1.1 MPa范围内较为合适,可将塔釜温度控制在80℃以下,在满足脱丙烷塔分离要求的前提下,减少因塔釜结焦造成的装置非计划停工。另外,文中从能耗和设备投资两方面对优化方案和常规方案进行了对比,优化方案能耗比常规方案降低约37%,主要设备投资也比常规方案低。 展开更多
关键词 催化裂解装置 液化石油气分离 脱丙烷塔 压力 温度 关键组分 相对挥发度 理论板数
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催化裂化装置消防安全措施的作用分析与研究 被引量:1
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作者 段弘磊 《当代化工研究》 CAS 2024年第1期107-109,共3页
催化裂化装置是石油化工生产中的关键设备,其所需的温度、压力等条件极其苛刻,而且存在着极高的火灾、爆炸风险。因此,对于催化裂化装置的消防安全问题必须高度重视。本文将从催化裂化装置的消防安全措施对安全性的作用进行分析和研究,... 催化裂化装置是石油化工生产中的关键设备,其所需的温度、压力等条件极其苛刻,而且存在着极高的火灾、爆炸风险。因此,对于催化裂化装置的消防安全问题必须高度重视。本文将从催化裂化装置的消防安全措施对安全性的作用进行分析和研究,旨在为石油化工生产中的催化裂化装置的消防安全提供一些借鉴意义。 展开更多
关键词 催化裂化装置 消防安全 安全性措施 借鉴意义
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催化裂化装置烟机振动异常情况的分析
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作者 王振南 刘甜甜 +4 位作者 王国刚 郭明 林瀚 张金庆 刘欣梅 《广州化工》 CAS 2024年第8期155-157,182,共4页
烟机振动导致的炼厂非计划停工对于炼厂来说是一大难题,本文通过对装置的运行情况分析,发现烟机导流锥、动静叶片上结了很多垢片,导致烟机振动剧烈,通过标准方法等动采样对烟机入口颗粒物浓度、颗粒物筛分分布及垢样化学组成进行分析,... 烟机振动导致的炼厂非计划停工对于炼厂来说是一大难题,本文通过对装置的运行情况分析,发现烟机导流锥、动静叶片上结了很多垢片,导致烟机振动剧烈,通过标准方法等动采样对烟机入口颗粒物浓度、颗粒物筛分分布及垢样化学组成进行分析,其大部分是催化剂细粉的共熔物,其Ni、V金属总含量在20 000 ppm以上,对此提出切实可行的措施,实现烟机的长周期运转。 展开更多
关键词 催化裂化装置 结垢振动 烟机 催化剂
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基于改进TOPSIS的石化装置实时状态评估
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作者 林扬 杨哲 +3 位作者 袁壮 苟成冬 李传坤 王春利 《石油炼制与化工》 CAS CSCD 北大核心 2024年第3期89-96,共8页
针对石化装置运行工况数据积累量有限,难以满足装置运行状态传统评估方法数据需求的问题,提出基于改进逼近理想解法(TOPSIS)的状态评估方法,避免了对装置历史运行数据的依赖。该基于改进TOPSIS的评估方法,首先根据现场专家经验和工艺卡... 针对石化装置运行工况数据积累量有限,难以满足装置运行状态传统评估方法数据需求的问题,提出基于改进逼近理想解法(TOPSIS)的状态评估方法,避免了对装置历史运行数据的依赖。该基于改进TOPSIS的评估方法,首先根据现场专家经验和工艺卡片过程指标的控制限,确定TOPSIS的正、负理想解;然后根据装置运行参数特点,形成固定值型和固定区间型指标,并建立相应的评估标准。采用该基于改进TOPSIS的评估方法对某炼油厂催化裂化装置反应-再生系统的异常工况进行了分析,结果表明该评估方法可以实现对催化裂化装置反应-再生系统的运行状态进行量化监测。 展开更多
关键词 逼近理想解法 石化装置 状态评估 健康指数 催化裂化装置
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DCC装置长周期运行工艺核算及技术分析
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作者 万涛 《石油炼制与化工》 CAS CSCD 北大核心 2024年第3期43-49,共7页
中海油东方石化有限责任公司(简称东方石化)增强型催化裂解(DCC-plus)装置的第二个生产运行周期内,装置原料性质变化频繁、操作工况调整较大,基于原料性质和催化剂性质,通过定期开展工艺核算及技术分析,调控原料预热温度、蒸汽注入量、... 中海油东方石化有限责任公司(简称东方石化)增强型催化裂解(DCC-plus)装置的第二个生产运行周期内,装置原料性质变化频繁、操作工况调整较大,基于原料性质和催化剂性质,通过定期开展工艺核算及技术分析,调控原料预热温度、蒸汽注入量、反应苛刻度、重点部位线速,稳定油浆系统操作参数,优化设备管理等,确保该装置在第二运行周期内未发生非计划停工情况,并成功实现了DCC-plus装置检修周期由3年延长至4年的突破。 展开更多
关键词 催化裂解装置 长周期运行 工艺核算 操作
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新一代防结焦沉降器的开发及应用
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作者 段丹 吴雷 +1 位作者 江盛阳 范声 《石油炼制与化工》 CAS CSCD 北大核心 2024年第4期53-57,共5页
沉降器内部结构对反应油气的流动状况和停留时间起决定性作用,沉降器内油气平均停留时间越长,就越容易结焦。中国石化工程建设有限公司针对以中间基劣质原油为原料的催化裂化装置的沉降器结焦问题及防结焦技术进行了系统研究,开发了新... 沉降器内部结构对反应油气的流动状况和停留时间起决定性作用,沉降器内油气平均停留时间越长,就越容易结焦。中国石化工程建设有限公司针对以中间基劣质原油为原料的催化裂化装置的沉降器结焦问题及防结焦技术进行了系统研究,开发了新一代防结焦沉降器并成功实现工业应用。新一代防结焦沉降器包括新一代全封闭旋流式快分系统、旋风分离系统升气管旋片和防焦蒸汽环等结构,可以大幅降低油气在沉降器内的停留时间,将油气限制在封闭罩内,防止油气弥散至沉降器内的其他空间,有效避免油气在沉降器内结焦,并且油剂分离效率高,油浆固含量显著降低,催化裂化装置运行周期延长。 展开更多
关键词 沉降器 旋风分离器 防结焦 重油催化裂化装置 旋流式快分
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重油催化裂化装置再生器衬里修复
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作者 钱继翔 尹发源 《石油化工设备》 CAS 2024年第5期70-75,共6页
催化裂化装置再生器和沉降器的过渡段及斜管入口处位置特殊,此处发生衬里损坏后的修复难度大。从衬里结构、衬里材料、施工措施等方面分析了衬里损坏的原因,提出并实施了针对性修复措施,修复后相关部位衬里损坏频率显著降低,有力保障了... 催化裂化装置再生器和沉降器的过渡段及斜管入口处位置特殊,此处发生衬里损坏后的修复难度大。从衬里结构、衬里材料、施工措施等方面分析了衬里损坏的原因,提出并实施了针对性修复措施,修复后相关部位衬里损坏频率显著降低,有力保障了催化裂化装置的平稳运行,可为类似检修、修补及设计提供参考。 展开更多
关键词 催化裂化装置 再生器 衬里 损坏 原因 修复
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催化裂化装置高温烟气管道焊缝开裂原因分析及应对措施
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作者 陈阳 《石油化工设备》 CAS 2024年第4期74-77,共4页
催化裂化装置第三旋风分离器至烟气轮机入口高温烟气管道为烟气能量回收系统的主要环节,对实现装置节能环保具有重要意义。根据某炼化公司催化裂化装置高温烟气管道焊缝开裂情况,从多方面对开裂原因进行了分析总结,认为低温露点腐蚀、... 催化裂化装置第三旋风分离器至烟气轮机入口高温烟气管道为烟气能量回收系统的主要环节,对实现装置节能环保具有重要意义。根据某炼化公司催化裂化装置高温烟气管道焊缝开裂情况,从多方面对开裂原因进行了分析总结,认为低温露点腐蚀、材料σ相脆化、高温蠕变、保温不当及应力集中等是造成管道开裂的主要原因。结合催化裂化装置运行实际情况,提出了加强焊缝、记录膨胀节及支吊架变形、改善保温以及选用适宜焊条等应对措施,对催化裂化装置的平稳运行具有借鉴意义。 展开更多
关键词 催化裂化装置 烟气管道 焊缝 开裂 高温
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催化裂化装置旋风分离器的锥体器壁磨损穿孔分析
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作者 孙立强 解明 +1 位作者 杨亮 彭威 《承德石油高等专科学校学报》 CAS 2024年第2期45-49,共5页
某1.0 Mt/a催化裂化装置在运行过程中,再生器旋风分离器的锥体发生了器壁磨损穿孔损坏。旋风分离器器壁磨损穿孔后导致分离效率下降,出现了比较严重的催化剂跑损故障。为此,依据气固两相流的磨损模型和气固旋流流场特点分析了磨损穿孔... 某1.0 Mt/a催化裂化装置在运行过程中,再生器旋风分离器的锥体发生了器壁磨损穿孔损坏。旋风分离器器壁磨损穿孔后导致分离效率下降,出现了比较严重的催化剂跑损故障。为此,依据气固两相流的磨损模型和气固旋流流场特点分析了磨损穿孔问题发生的过程。催化剂在旋风分离器内部的离心力和重力的作用下聚集在器壁表面形成了下行的螺旋灰环。当螺旋灰环运动到锥体段时,灰环的加速旋转流动使灰环螺旋角减小,在器壁表面形成一个悬浮的旋转灰环,同时灰环的颗粒浓度也增大,对器壁的正压力增大,导致对器壁摩擦作用增强,最后造成锥体器壁的磨损穿孔。 展开更多
关键词 催化裂化装置 旋风分离器 磨损 穿孔
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