To reduce CO_(2) emissions from coal-fired power plants,the development of low-carbon or carbon-free fuel combustion technologies has become urgent.As a new zero-carbon fuel,ammonia(NH_(3))can be used to address the s...To reduce CO_(2) emissions from coal-fired power plants,the development of low-carbon or carbon-free fuel combustion technologies has become urgent.As a new zero-carbon fuel,ammonia(NH_(3))can be used to address the storage and transportation issues of hydrogen energy.Since it is not feasible to completely replace coal with ammonia in the short term,the development of ammonia-coal co-combustion technology at the current stage is a fast and feasible approach to reduce CO_(2) emissions from coal-fired power plants.This study focuses on modifying the boiler and installing two layers of eight pure-ammonia burners in a 300-MW coal-fired power plant to achieve ammonia-coal co-combustion at proportions ranging from 20%to 10%(by heat ratio)at loads of 180-to 300-MW,respectively.The results show that,during ammonia-coal co-combustion in a 300-MW coal-fired power plant,there was a more significant change in NO_(x) emissions at the furnace outlet compared with that under pure-coal combustion as the boiler oxygen levels varied.Moreover,ammonia burners located in the middle part of the main combustion zone exhibited a better high-temperature reduction performance than those located in the upper part of the main combustion zone.Under all ammonia co-combustion conditions,the NH_(3) concentration at the furnace outlet remained below 1 parts per million(ppm).Compared with that under pure-coal conditions,the thermal efficiency of the boiler slightly decreased(by 0.12%-0.38%)under different loads when ammonia co-combustion reached 15 t·h^(-1).Ammonia co-combustion in coal-fired power plants is a potentially feasible technology route for carbon reduction.展开更多
A 600 MW coal-fired boiler with a four-corner tangential combustion mode is considered here to study the combustion features and pollutant emissions at different loads for large-percentages of blending dried sludges.T...A 600 MW coal-fired boiler with a four-corner tangential combustion mode is considered here to study the combustion features and pollutant emissions at different loads for large-percentages of blending dried sludges.The influence of the over-fired air(OFA)coefficient is examined and the impact of the blending ratio on the boiler operation is explored.The results show that for low blending ratios,a slight increase in the blending ratio can improve the combustion of bituminite,whereas a further increase leads to the deterioration of the combustion of blended fuels and thus reduces the boiler efficiency.Enhancing the supporting capability of the secondary air effectively reduces the slagging degree in the bottom ash hopper and improves the burnout rate of coals.For a large-percentage blending case at full load,it is found that the OFA coefficient must be reduced appropriately,otherwise,a secondary high-temperature combustion zone can be generated in the vicinity of the furnace arches,causing high temperature slagging and superheater tube bursting.Considering the influences of combustion and pollutant emissions,the recommended OFA coefficient is 0.2.Blending dried sludge under low loads increases the flue gas temperature at the furnace exit.While reducing the flue gas temperature in the main combustion region,which is beneficial to the safe operation of the denitrification system.Increasing the blending ratio and reducing load lead to an increase in NOx concentration at the furnace exit Sludges with low nitrogen content are suggested for the practical operation of boilers.展开更多
Chinese utilities as well as those worldwide are facing increased demand for additional electricity, reduced plant emissions and greater efficiency. To meet this challenge will require increasing boiler temperature, p...Chinese utilities as well as those worldwide are facing increased demand for additional electricity, reduced plant emissions and greater efficiency. To meet this challenge will require increasing boiler temperature, pressure and coal ash corrosion resistance of the materials of boiler construction of future coal-fired boilers. A new nickel-based tube alloy, INCONEL^R alloy 740, is described aiming at meeting this challenge. Emphasis will be on describing the alloy' s mechanical properties, coal-ash and steam corrosion resistance. Microstructural stability as a function of temperature and time is addressed as well as some of the early methodology em- ployed to arrive at the current chemical composition.展开更多
To implement a real-time reduction in NOx,a rapid and accurate model is required.A PLS-ELM model based on the combination of partial least squares(PLS)and the extreme learning machine(ELM)for the establishment of the ...To implement a real-time reduction in NOx,a rapid and accurate model is required.A PLS-ELM model based on the combination of partial least squares(PLS)and the extreme learning machine(ELM)for the establishment of the NOx emission model of utility boilers is proposed.First,the initial input variables of the NOx emission model are determined according to the mechanism analysis.Then,the initial input data is extracted by PLS.Finally,the extracted information is used as the input of the ELM model.A large amount of real data was obtained from the distributed control system(DCS)historical database of a 1 000 MW power plant boiler to train and validate the PLS-ELM model.The modeling performance of the PLS-ELM was compared with that of the back propagation(BP)neural network,support vector machine(SVM)and ELM models.The mean relative errors(MRE)of the PLS-ELM model were 1.58%for the training dataset and 1.69%for the testing dataset.The prediction precision of the PLS-ELM model is higher than those of the BP,SVM and ELM models.The consumption time of the PLS-ELM model is also shorter than that of the BP,SVM and ELM models.展开更多
The feasibility of adopting a balanced energy mix mode (domestic solar energy, biogas, coal-fired boiler and radiant floor heating) was proposed. Taking a typical rural residence in Zhengzhou City for example, the stu...The feasibility of adopting a balanced energy mix mode (domestic solar energy, biogas, coal-fired boiler and radiant floor heating) was proposed. Taking a typical rural residence in Zhengzhou City for example, the study through theoretical analysis and calculation showed that such a balanced energy mix is an economic way and efficient in saving energy and reducing air pollution, and elaborated the theoretical feasibility of popularizing such a heat supply mode in rural areas.展开更多
Since the combustion system of coal-fired boiler in thermal power plant is characterized as time varying, strongly coupled, and nonlinear, it is hard to achieve a satisfactory performance by the conventional proportio...Since the combustion system of coal-fired boiler in thermal power plant is characterized as time varying, strongly coupled, and nonlinear, it is hard to achieve a satisfactory performance by the conventional proportional integral derivative (PID) control scheme. For the characteristics of the main steam pressure in coal-fired power plant boiler, the sliding mode control system with Smith predictive structure is proposed to look for performance and robustness improvement. First, internal model control (IMC) and Smith predictor (SP) is used to deal with the time delay, and sliding mode controller (SMCr) is designed to overcome the model mismatch. Simulation results show the effectiveness of the proposed controller compared with conventional ones.展开更多
To reduce greenhouse gases emission and increase the renewable energy uti</span><span style="font-family:Verdana;">lization portion in the world, the biomass gasification coupled with a coal-fire...To reduce greenhouse gases emission and increase the renewable energy uti</span><span style="font-family:Verdana;">lization portion in the world, the biomass gasification coupled with a coal-fired </span><span style="font-family:Verdana;">boiler power generation system is studied. It is a challenge to achieve optimum performance for the coupled system. The models of biomass gasification coupled with co-firing of coal in a boiler have been established. A comparative study of three kinds of biomass (Food Rubbish, Straw and Wood Pellets) has </span></span></span><span style="font-family:Verdana;"><span style="font-family:Verdana;"><span style="font-family:Verdana;">been </span></span></span><span><span><span><span style="font-family:Verdana;">done. The syngas produced in a 10 t/h gasifier is fed to a 330 MWe coal-fired boiler for co-combustion, and the co-firing performances have been compared with pure coal combustion case under the conditions of constant boiler load. Results show that co-firing decreases the furnace combustion temperature and raises the flue gas temperature for Food Rubbish and Straw, while, flue gases temperature decrease in case of Wood Pellets. At the same time NO<sub>x</sub> and SO<sub>x</sub> emissions have reduced. The system efficiencies at constant load for Food Rubbish, Straw and Wood Pellets are 83.25%, </span><span style="font-family:Verdana;">83.88% and 82.56% when the optimum conditions of gasification and co-firing </span><span style="font-family:Verdana;">process are guaranteed.展开更多
One of the pathways for achieving the goal of increasing the efficiency of coal-fired power plants and reducing the emission of pollutants and CO_2 is by improving the steam temperature and pressure.But the increase o...One of the pathways for achieving the goal of increasing the efficiency of coal-fired power plants and reducing the emission of pollutants and CO_2 is by improving the steam temperature and pressure.But the increase of steam parameters depend on the development of new high-temperature metal materials.This paper presented the constructive suggestions on critical materials selection for China's new generation of 700℃clean and high-efficiency coal-fired boiler by summarizing the research and development situation of critical materials for coal-fired boilers operating at 700℃/35 MPa of the Europe,Japan and USA.展开更多
The Paper has introduced development of domesticand foreign coal-fired industry boiler and has implementedcomprehensive comparison for several substitution technologies(coal powder boiler, coal water mixture boiler, ...The Paper has introduced development of domesticand foreign coal-fired industry boiler and has implementedcomprehensive comparison for several substitution technologies(coal powder boiler, coal water mixture boiler, coal-fired boiler,gas-fired boiler and biomass boiler, etc.) of backward coal-firedindustrial boiler in technology, economy and environment, etc.;has evaluated comprehensive effect and adaptiveconditions of coal-fired industry boiler technology and has put forward suggestion forefficient development of coal-fired industry boiler clearing.展开更多
In this paper, FLUENT software was used to simulate the burning process in a utility boiler. Chose the kinetics/diffusion-limited as combustion model, two-competing-rates as devolatilization model, RNG k-εmodel as vi...In this paper, FLUENT software was used to simulate the burning process in a utility boiler. Chose the kinetics/diffusion-limited as combustion model, two-competing-rates as devolatilization model, RNG k-εmodel as viscous model, and PDF model as combustion turbulent flow model. Numerical calculation of NOx formation in a 330 MW cyclone-opposed coal-fired utility boiler with 32 double air registers was done. The distribution characteristics of temperature, NOx and oxygen concentration in furnace were studied. They were symmetrically distributed in furnace. In the combustion area, temperature and NOx concentration are high, while oxygen concentration is low. Temperature and NOx concentration are declined gradually along with furnace height, while oxygen concentration is raised. The higher the temperature is and the greater the excess air coefficient is, the more NOx formation.展开更多
Based on the investigation of NOx formation mechanism, a coal-fired utility boiler whose capacity is 1 004 t/h was studied. Excessive air coefficient, inclination of burner and the way of coal supply were investigated...Based on the investigation of NOx formation mechanism, a coal-fired utility boiler whose capacity is 1 004 t/h was studied. Excessive air coefficient, inclination of burner and the way of coal supply were investigated through experimental method. Resuits indicated that under the condition of same boiler efficiency and burn-off rate, the operation conditions adopting the lower excessive air coefficient, upward burners' inclination and pyramid coal-supply could reduce NOx emission.展开更多
This article reviews the problems of Russia-made 800-MW coal-fired supercritical boilers in Suizhong Power Plant, such as burner bumout, water-wall leakage, slag screenⅠexplosion, crack happened on the desuperheater ...This article reviews the problems of Russia-made 800-MW coal-fired supercritical boilers in Suizhong Power Plant, such as burner bumout, water-wall leakage, slag screenⅠexplosion, crack happened on the desuperheater outlet of reheater and welding defect of economizer; tells the process of renovating these units by modifying the original design and adjusting the operation parameters. After several years' effort, all the problems have been well solved. The experience may be useful for other imported units in China.展开更多
A liquid-solid circulating fluidized bed boiler is designed and built for visualization research by applying the fluidized bed heat transfer and fouling prevention technology to the water side of the boiler. Four type...A liquid-solid circulating fluidized bed boiler is designed and built for visualization research by applying the fluidized bed heat transfer and fouling prevention technology to the water side of the boiler. Four types of engineering plastic particles with different physical properties are selected as the solid working media. The effect of particle types on the fluidization and distribution of particles in the boiler is investigated under different feedwater flow rates and amount of added particles by using the charge couple device image measurement and acquisition system. The results show that all kinds of particles can't be normally fluidized and accumulate in the drum at low amount of added particles and feedwater flow rate. The particles with great density and low sphericity are more likely to accumulate. The average solid holdup in the riser tubes increases with the increase in feedwater flow rate and the amount of added particles. The non-uniform degree of particle distribution in the riser tubes generally decreases with the increase in feedwater flow rate and the amount of added particles. The particles with small density and settling velocity have high average solid holdup in the riser tubes under close sphericity. In generally,the smaller the density and settling velocity, the more uniform the particle distribution in the riser tubes.Three-dimensional diagrams of the non-uniform degree of particle distribution in the riser tubes of the boiler are established.展开更多
The purpose of this article is to receive environmental assessments of combustion of different types of coal fuel depending on the preparation(unscreened,size-graded,briquetted and heat-treated)in automated boilers an...The purpose of this article is to receive environmental assessments of combustion of different types of coal fuel depending on the preparation(unscreened,size-graded,briquetted and heat-treated)in automated boilers and boilers with manual load-ing.The assessments were made on the basis of data obtained from experimental methods of coal preparation and calculated methods of determining the amount of pollutant and greenhouse gas emissions,as well as the mass of ash and slag waste.The main pollutants from coal combustion are calculated:particulate matter,benz(a)pyrene,nitrogen oxides,sulfur dioxide,carbon monoxide.Of the greenhouse gases carbon dioxide is calculated.As a result of conducted research it is shown that the simplest preliminary preparation(size-graded)of coal significantly improves combustion efficiency and environmental performance:emissions are reduced by 13%for hard coal and up to 20%for brown coal.The introduction of automated boil-ers with heat-treated coal in small boiler facilities allows to reduce emissions and ash and slag waste by 2-3 times.The best environmental indicators correspond to heat-treated lignite,which is characterized by the absence of sulfur dioxide emissions.展开更多
Coal has been dominating the electricity supply in Indonesia,especially in long-term power generation from fossil energy.This dominance is due to lower production costs in coal-fired power plant generation.However,thi...Coal has been dominating the electricity supply in Indonesia,especially in long-term power generation from fossil energy.This dominance is due to lower production costs in coal-fired power plant generation.However,this low price is only based on monetary costs and ignores the social costs.Therefore,this study aims to quantify the social costs of coal-fired generation.Using QUERI-AirPacts modeling,the present study quantifies the social costs resulting from the Tenayan Raya coal-fired generation in Riau,Indonesia.It includes the levelized cost of electricity and health costs into the generation costs.After that,this study calculates the net present value,internal rate return,and project payback period.The study found that as much as$50.22/MWh was the levelized cost of electricity.While$15.978/MWh or$0.015978/kWh was the social cost that was not included in the generating cost.At the electricity production level of 1,380,171.69 MWh per year,there is an expected extra cost of$22,052,383.30 uncounted when externalities are included.For instance,the net present value(NPV)is lower and even negative when external costs are included(-$24,062,274.19)compared to$176,108,091.52 when externalities are not considered.The internal rate of return(IRR)is much higher when the social costs are not considered.The payback period is also shorter when the social costs are excluded than when the externalities are included.This global number indicates that the inclusion of external costs would impact NPV,IRR,and the payback period.This result implies that the government should internalize the external cost to stimulate the electricity producers to conduct cost-benefit analyses.The cost-benefit analysis mechanism would lead the producers to be more efficient.展开更多
The hazardous waste produced by coal-fired power plants are large in quantity and variety. It is important for ecological environment protection to properly store hazardous waste in coal-fired power plants. The enviro...The hazardous waste produced by coal-fired power plants are large in quantity and variety. It is important for ecological environment protection to properly store hazardous waste in coal-fired power plants. The environmental management of hazardous waste in coal-fired power plants started late, and there are many problems in the construction and management of their storage facilities. In this paper, taking eight typical coal-fired power plants as examples, the present problems of hazardous waste storage facilities in coal-fired power plants are analyzed, and corresponding countermeasures are put forward to solve the main common problems.展开更多
Supercritical carbon dioxide(S-CO_(2))Brayton power cycle power generation technology,has attracted more and more scholars'attention in recent years because of its advantages of high efficiency and flexibility.Com...Supercritical carbon dioxide(S-CO_(2))Brayton power cycle power generation technology,has attracted more and more scholars'attention in recent years because of its advantages of high efficiency and flexibility.Compared with conventional steam boilers,S-CO_(2) has different heat transfer characteristics,it is easy to cause the temperature of the cooling wall of the boiler to rise,which leads to higher combustion gas temperature in the furnace,higher NOX generation concentration.The adoption of flue gas recirculation has a significance impact on the combustion process of pulverized coal in the boiler,and it is the most effective ways to reduce the emission of NOX and the combustion temperature in the boiler.This paper takes 1000MW S-CO_(2) T-type coal-fired boiler as the research target to investigate the combustion and NOX generation characteristics of S-CO_(2) coal-fired boilers under flue gas recirculation condition,the influence of recirculated flue gas distribution along the furnace height on the characteristics of NOX formation and the combustion of pulverized coal.The results show that the recirculated flue gas distribution has the great impact on the concentration of NOX at the boiler outlet.When the bottom recirculation flue gas rate is gradually increased,the average temperature of the lower boiler decreases and the average temperature of the upper boiler increases slightly;The concentration of NOx at the furnace outlet increases.展开更多
基金supported by the National Key Research and Development Program of China(2023YFB4005700,2023YFB4005705,and 2023YFB4005702-03)the Academy-Local Cooperation Project of the Chinese Academy of Engineering(2023-DFZD-01)+4 种基金the National Natural Science Foundation of China(52207151)the Natural Science Foundation of Anhui Province(2208085QA29)the University Synergy Innovation Program of Anhui Province(GXXT-2022025)the independent project of the Energy Research Institute of Hefei Comprehensive National Science Center(Anhui Energy Laboratory22KZZ525,23KZS402,22KZS301,and 22KZS304).
文摘To reduce CO_(2) emissions from coal-fired power plants,the development of low-carbon or carbon-free fuel combustion technologies has become urgent.As a new zero-carbon fuel,ammonia(NH_(3))can be used to address the storage and transportation issues of hydrogen energy.Since it is not feasible to completely replace coal with ammonia in the short term,the development of ammonia-coal co-combustion technology at the current stage is a fast and feasible approach to reduce CO_(2) emissions from coal-fired power plants.This study focuses on modifying the boiler and installing two layers of eight pure-ammonia burners in a 300-MW coal-fired power plant to achieve ammonia-coal co-combustion at proportions ranging from 20%to 10%(by heat ratio)at loads of 180-to 300-MW,respectively.The results show that,during ammonia-coal co-combustion in a 300-MW coal-fired power plant,there was a more significant change in NO_(x) emissions at the furnace outlet compared with that under pure-coal combustion as the boiler oxygen levels varied.Moreover,ammonia burners located in the middle part of the main combustion zone exhibited a better high-temperature reduction performance than those located in the upper part of the main combustion zone.Under all ammonia co-combustion conditions,the NH_(3) concentration at the furnace outlet remained below 1 parts per million(ppm).Compared with that under pure-coal conditions,the thermal efficiency of the boiler slightly decreased(by 0.12%-0.38%)under different loads when ammonia co-combustion reached 15 t·h^(-1).Ammonia co-combustion in coal-fired power plants is a potentially feasible technology route for carbon reduction.
文摘A 600 MW coal-fired boiler with a four-corner tangential combustion mode is considered here to study the combustion features and pollutant emissions at different loads for large-percentages of blending dried sludges.The influence of the over-fired air(OFA)coefficient is examined and the impact of the blending ratio on the boiler operation is explored.The results show that for low blending ratios,a slight increase in the blending ratio can improve the combustion of bituminite,whereas a further increase leads to the deterioration of the combustion of blended fuels and thus reduces the boiler efficiency.Enhancing the supporting capability of the secondary air effectively reduces the slagging degree in the bottom ash hopper and improves the burnout rate of coals.For a large-percentage blending case at full load,it is found that the OFA coefficient must be reduced appropriately,otherwise,a secondary high-temperature combustion zone can be generated in the vicinity of the furnace arches,causing high temperature slagging and superheater tube bursting.Considering the influences of combustion and pollutant emissions,the recommended OFA coefficient is 0.2.Blending dried sludge under low loads increases the flue gas temperature at the furnace exit.While reducing the flue gas temperature in the main combustion region,which is beneficial to the safe operation of the denitrification system.Increasing the blending ratio and reducing load lead to an increase in NOx concentration at the furnace exit Sludges with low nitrogen content are suggested for the practical operation of boilers.
文摘Chinese utilities as well as those worldwide are facing increased demand for additional electricity, reduced plant emissions and greater efficiency. To meet this challenge will require increasing boiler temperature, pressure and coal ash corrosion resistance of the materials of boiler construction of future coal-fired boilers. A new nickel-based tube alloy, INCONEL^R alloy 740, is described aiming at meeting this challenge. Emphasis will be on describing the alloy' s mechanical properties, coal-ash and steam corrosion resistance. Microstructural stability as a function of temperature and time is addressed as well as some of the early methodology em- ployed to arrive at the current chemical composition.
基金The National Natural Science Foundation of China(No.71471060)Natural Science Foundation of Hebei Province(No.E2018502111)
文摘To implement a real-time reduction in NOx,a rapid and accurate model is required.A PLS-ELM model based on the combination of partial least squares(PLS)and the extreme learning machine(ELM)for the establishment of the NOx emission model of utility boilers is proposed.First,the initial input variables of the NOx emission model are determined according to the mechanism analysis.Then,the initial input data is extracted by PLS.Finally,the extracted information is used as the input of the ELM model.A large amount of real data was obtained from the distributed control system(DCS)historical database of a 1 000 MW power plant boiler to train and validate the PLS-ELM model.The modeling performance of the PLS-ELM was compared with that of the back propagation(BP)neural network,support vector machine(SVM)and ELM models.The mean relative errors(MRE)of the PLS-ELM model were 1.58%for the training dataset and 1.69%for the testing dataset.The prediction precision of the PLS-ELM model is higher than those of the BP,SVM and ELM models.The consumption time of the PLS-ELM model is also shorter than that of the BP,SVM and ELM models.
基金Supported by Key Scientific Research Projects of Sichuan Provincial Department of Technology (2010JY0165)Key Special Scientific Research Projects of Mianyang City of Sichuan Province (09Y003-13)Key Scientific Research Projects of Sichuan Provincial Department of Education (2003A112)
文摘The feasibility of adopting a balanced energy mix mode (domestic solar energy, biogas, coal-fired boiler and radiant floor heating) was proposed. Taking a typical rural residence in Zhengzhou City for example, the study through theoretical analysis and calculation showed that such a balanced energy mix is an economic way and efficient in saving energy and reducing air pollution, and elaborated the theoretical feasibility of popularizing such a heat supply mode in rural areas.
基金Supported by the National Natural Science Foundation of China (61174059, 60934007, 61233004)the National Basic Research Program of China (2013CB035406)Shanghai Rising-Star Tracking Program (11QH1401300)
文摘Since the combustion system of coal-fired boiler in thermal power plant is characterized as time varying, strongly coupled, and nonlinear, it is hard to achieve a satisfactory performance by the conventional proportional integral derivative (PID) control scheme. For the characteristics of the main steam pressure in coal-fired power plant boiler, the sliding mode control system with Smith predictive structure is proposed to look for performance and robustness improvement. First, internal model control (IMC) and Smith predictor (SP) is used to deal with the time delay, and sliding mode controller (SMCr) is designed to overcome the model mismatch. Simulation results show the effectiveness of the proposed controller compared with conventional ones.
文摘To reduce greenhouse gases emission and increase the renewable energy uti</span><span style="font-family:Verdana;">lization portion in the world, the biomass gasification coupled with a coal-fired </span><span style="font-family:Verdana;">boiler power generation system is studied. It is a challenge to achieve optimum performance for the coupled system. The models of biomass gasification coupled with co-firing of coal in a boiler have been established. A comparative study of three kinds of biomass (Food Rubbish, Straw and Wood Pellets) has </span></span></span><span style="font-family:Verdana;"><span style="font-family:Verdana;"><span style="font-family:Verdana;">been </span></span></span><span><span><span><span style="font-family:Verdana;">done. The syngas produced in a 10 t/h gasifier is fed to a 330 MWe coal-fired boiler for co-combustion, and the co-firing performances have been compared with pure coal combustion case under the conditions of constant boiler load. Results show that co-firing decreases the furnace combustion temperature and raises the flue gas temperature for Food Rubbish and Straw, while, flue gases temperature decrease in case of Wood Pellets. At the same time NO<sub>x</sub> and SO<sub>x</sub> emissions have reduced. The system efficiencies at constant load for Food Rubbish, Straw and Wood Pellets are 83.25%, </span><span style="font-family:Verdana;">83.88% and 82.56% when the optimum conditions of gasification and co-firing </span><span style="font-family:Verdana;">process are guaranteed.
文摘One of the pathways for achieving the goal of increasing the efficiency of coal-fired power plants and reducing the emission of pollutants and CO_2 is by improving the steam temperature and pressure.But the increase of steam parameters depend on the development of new high-temperature metal materials.This paper presented the constructive suggestions on critical materials selection for China's new generation of 700℃clean and high-efficiency coal-fired boiler by summarizing the research and development situation of critical materials for coal-fired boilers operating at 700℃/35 MPa of the Europe,Japan and USA.
文摘The Paper has introduced development of domesticand foreign coal-fired industry boiler and has implementedcomprehensive comparison for several substitution technologies(coal powder boiler, coal water mixture boiler, coal-fired boiler,gas-fired boiler and biomass boiler, etc.) of backward coal-firedindustrial boiler in technology, economy and environment, etc.;has evaluated comprehensive effect and adaptiveconditions of coal-fired industry boiler technology and has put forward suggestion forefficient development of coal-fired industry boiler clearing.
基金Supported by Major Project of Tackle Key Problems of Shanghai (Z2003-1)
文摘In this paper, FLUENT software was used to simulate the burning process in a utility boiler. Chose the kinetics/diffusion-limited as combustion model, two-competing-rates as devolatilization model, RNG k-εmodel as viscous model, and PDF model as combustion turbulent flow model. Numerical calculation of NOx formation in a 330 MW cyclone-opposed coal-fired utility boiler with 32 double air registers was done. The distribution characteristics of temperature, NOx and oxygen concentration in furnace were studied. They were symmetrically distributed in furnace. In the combustion area, temperature and NOx concentration are high, while oxygen concentration is low. Temperature and NOx concentration are declined gradually along with furnace height, while oxygen concentration is raised. The higher the temperature is and the greater the excess air coefficient is, the more NOx formation.
基金Supported by the Youth Fundation of Shanghai University of Electric Power (F2004016)Shanghai Leading Academic Discipline Project (P1302)
文摘Based on the investigation of NOx formation mechanism, a coal-fired utility boiler whose capacity is 1 004 t/h was studied. Excessive air coefficient, inclination of burner and the way of coal supply were investigated through experimental method. Resuits indicated that under the condition of same boiler efficiency and burn-off rate, the operation conditions adopting the lower excessive air coefficient, upward burners' inclination and pyramid coal-supply could reduce NOx emission.
文摘This article reviews the problems of Russia-made 800-MW coal-fired supercritical boilers in Suizhong Power Plant, such as burner bumout, water-wall leakage, slag screenⅠexplosion, crack happened on the desuperheater outlet of reheater and welding defect of economizer; tells the process of renovating these units by modifying the original design and adjusting the operation parameters. After several years' effort, all the problems have been well solved. The experience may be useful for other imported units in China.
基金supported by the open foundation of State Key Laboratory of Chemical Engineering (SKL–ChE–18B03)the Municipal Science and Technology Commission of Tianjin, China (2009ZCKFGX01900)。
文摘A liquid-solid circulating fluidized bed boiler is designed and built for visualization research by applying the fluidized bed heat transfer and fouling prevention technology to the water side of the boiler. Four types of engineering plastic particles with different physical properties are selected as the solid working media. The effect of particle types on the fluidization and distribution of particles in the boiler is investigated under different feedwater flow rates and amount of added particles by using the charge couple device image measurement and acquisition system. The results show that all kinds of particles can't be normally fluidized and accumulate in the drum at low amount of added particles and feedwater flow rate. The particles with great density and low sphericity are more likely to accumulate. The average solid holdup in the riser tubes increases with the increase in feedwater flow rate and the amount of added particles. The non-uniform degree of particle distribution in the riser tubes generally decreases with the increase in feedwater flow rate and the amount of added particles. The particles with small density and settling velocity have high average solid holdup in the riser tubes under close sphericity. In generally,the smaller the density and settling velocity, the more uniform the particle distribution in the riser tubes.Three-dimensional diagrams of the non-uniform degree of particle distribution in the riser tubes of the boiler are established.
基金The research was carried out under State Assignment Projects(FWEU-2021-0004,FWEU-2021-0005)of the Fundamental Research Program of Russian Federation 2021-2030.
文摘The purpose of this article is to receive environmental assessments of combustion of different types of coal fuel depending on the preparation(unscreened,size-graded,briquetted and heat-treated)in automated boilers and boilers with manual load-ing.The assessments were made on the basis of data obtained from experimental methods of coal preparation and calculated methods of determining the amount of pollutant and greenhouse gas emissions,as well as the mass of ash and slag waste.The main pollutants from coal combustion are calculated:particulate matter,benz(a)pyrene,nitrogen oxides,sulfur dioxide,carbon monoxide.Of the greenhouse gases carbon dioxide is calculated.As a result of conducted research it is shown that the simplest preliminary preparation(size-graded)of coal significantly improves combustion efficiency and environmental performance:emissions are reduced by 13%for hard coal and up to 20%for brown coal.The introduction of automated boil-ers with heat-treated coal in small boiler facilities allows to reduce emissions and ash and slag waste by 2-3 times.The best environmental indicators correspond to heat-treated lignite,which is characterized by the absence of sulfur dioxide emissions.
文摘Coal has been dominating the electricity supply in Indonesia,especially in long-term power generation from fossil energy.This dominance is due to lower production costs in coal-fired power plant generation.However,this low price is only based on monetary costs and ignores the social costs.Therefore,this study aims to quantify the social costs of coal-fired generation.Using QUERI-AirPacts modeling,the present study quantifies the social costs resulting from the Tenayan Raya coal-fired generation in Riau,Indonesia.It includes the levelized cost of electricity and health costs into the generation costs.After that,this study calculates the net present value,internal rate return,and project payback period.The study found that as much as$50.22/MWh was the levelized cost of electricity.While$15.978/MWh or$0.015978/kWh was the social cost that was not included in the generating cost.At the electricity production level of 1,380,171.69 MWh per year,there is an expected extra cost of$22,052,383.30 uncounted when externalities are included.For instance,the net present value(NPV)is lower and even negative when external costs are included(-$24,062,274.19)compared to$176,108,091.52 when externalities are not considered.The internal rate of return(IRR)is much higher when the social costs are not considered.The payback period is also shorter when the social costs are excluded than when the externalities are included.This global number indicates that the inclusion of external costs would impact NPV,IRR,and the payback period.This result implies that the government should internalize the external cost to stimulate the electricity producers to conduct cost-benefit analyses.The cost-benefit analysis mechanism would lead the producers to be more efficient.
文摘The hazardous waste produced by coal-fired power plants are large in quantity and variety. It is important for ecological environment protection to properly store hazardous waste in coal-fired power plants. The environmental management of hazardous waste in coal-fired power plants started late, and there are many problems in the construction and management of their storage facilities. In this paper, taking eight typical coal-fired power plants as examples, the present problems of hazardous waste storage facilities in coal-fired power plants are analyzed, and corresponding countermeasures are put forward to solve the main common problems.
基金This paper is supported by the National Key R&D Program of China(2017YFB0601805).
文摘Supercritical carbon dioxide(S-CO_(2))Brayton power cycle power generation technology,has attracted more and more scholars'attention in recent years because of its advantages of high efficiency and flexibility.Compared with conventional steam boilers,S-CO_(2) has different heat transfer characteristics,it is easy to cause the temperature of the cooling wall of the boiler to rise,which leads to higher combustion gas temperature in the furnace,higher NOX generation concentration.The adoption of flue gas recirculation has a significance impact on the combustion process of pulverized coal in the boiler,and it is the most effective ways to reduce the emission of NOX and the combustion temperature in the boiler.This paper takes 1000MW S-CO_(2) T-type coal-fired boiler as the research target to investigate the combustion and NOX generation characteristics of S-CO_(2) coal-fired boilers under flue gas recirculation condition,the influence of recirculated flue gas distribution along the furnace height on the characteristics of NOX formation and the combustion of pulverized coal.The results show that the recirculated flue gas distribution has the great impact on the concentration of NOX at the boiler outlet.When the bottom recirculation flue gas rate is gradually increased,the average temperature of the lower boiler decreases and the average temperature of the upper boiler increases slightly;The concentration of NOx at the furnace outlet increases.