Because the mover and stator of a doubly-fed linear motor are both equipped with three-phase windings, the motor enables contactless energy to be transferred from the stator to the mover. Thus, when a doubly-fed linea...Because the mover and stator of a doubly-fed linear motor are both equipped with three-phase windings, the motor enables contactless energy to be transferred from the stator to the mover. Thus, when a doubly-fed linear motor is used in the linear driving system of trains, neither an overhead line nor a third rail is needed. However, the doubly- fed motor will lead to more severe thrust fluctuation than the unilateral motors. In order to overcome this shortcoming, the thrust fluctuation of the doubly-fed motor should be analyzed. In this paper, an expression for motor thrust is derived. It points out that the slot effect caused by the slotted structure is the main reason for the increase of thrust fluctuation. The method of adopting unequal pole pitch and unequal slot numbers per pole per phase of stator and mover, is proposed to weaken the slot effect when designing the motor slot parameters. Three different motor models are simulated by ANSOFT. The proposed method results in a motor thrust fluctuation coefficient of 8.4%, compared to 49.4% for the conventional method. Therefore, the motor's thrust fluctuation is effectively suppressed by the proposed method.展开更多
The requirement of low radiated noise is increasing for underwater propulsors as the noise significantly affecting the comfort and quietness of ships,submarines,and vessels.To broaden the view of noise characteristics...The requirement of low radiated noise is increasing for underwater propulsors as the noise significantly affecting the comfort and quietness of ships,submarines,and vessels.To broaden the view of noise characteristics of pump-jet propulsors(PJPs),this paper considers the radiated noise of a pre-swirl stator PJP with the effects of the advance coefficient and rotor rotational speed.Radiated noise is obtained by the“hybrid method”approach,which combines a hydrodynamic solver with a hydroacoustic solver.The turbulence flow is obtained through improved delayed detached eddy simulation(IDDES),which show good agreement with the experiment,including the performance and flow field.The solver precision,permeable surface size,and sampling frequency notably affect the noise calculation.The spectra of thrust fluctuation and radiated noise are characterized by the tonal phenomenon around the blade passing frequency and its harmonics.The spectrum of radiated noise and overall sound pressure level(OSPL)are considerably affected by both the advance coefficient and the rotor rotational speed.Overall,the numerical results and analysis given in this paper should be partly helpful in deepening the understanding of the radiated noise characteristics of PJPs.展开更多
For a new type of toroidal permanent magnet linear motor(TPMLSM), this paper analyzes the thrust fluctuation in the constant acceleration operation of the motor from the Angle of the cogging force of the linear motor....For a new type of toroidal permanent magnet linear motor(TPMLSM), this paper analyzes the thrust fluctuation in the constant acceleration operation of the motor from the Angle of the cogging force of the linear motor. For the motor whose structure has been determined and processed, the structural parameters of the motor cannot be changed, and its performance cannot be improved from the perspective of the motor body.Therefore, this paper tries to consider the influence of the cogging force on the normal operation of the motor from the perspective of control. In this paper, starting from the body structure of motor, first on the annular linear motor of the cogging force characteristics were extracted, and its expression is obtained by Fourier decomposition, then investigated considering the cogging force and does not consider the cogging force control of motor model, it can be seen that the control performance deteriorates significantly after considering cogging force of the motor, and the acceleration fluctuation increases significantly during the operation of the motor. On this basis, disturbance observation algorithm is introduced, and feedforward compensation is carried out by extracting the characteristic values of the disturbance model. The results show that the disturbance observer can suppress the thrust fluctuation caused by the motor cogging force to a large extent, and it can reduce the peak-to-peak value of the thrust fluctuation by more than 85% during the motor acceleration operation.展开更多
Ducted fans have been extensively used in Unmanned Aerial Vehicles(UAVs)for a variety of missions because of high efficiency,high safety and low noise.Wind,as a kind of typical meteorological condition,brings signific...Ducted fans have been extensively used in Unmanned Aerial Vehicles(UAVs)for a variety of missions because of high efficiency,high safety and low noise.Wind,as a kind of typical meteorological condition,brings significant aerodynamic interference to the ducted fan,which seriously threatens flight stability and safety.In this work,the numerical simulation with the Unsteady Reynolds Averaged Navier-Stokes(URANS)method and the sliding mesh technique is performed to evaluate the steady wind effect.The results show that the wind will lead to serious unsteady effects in the flow field,and the thrust fluctuates at the blade passing frequency of 200 Hz.As the wind speed increases,the rotor thrust increases,the duct thrust decreases,and the total thrust changes little.Flow instability may occur when the wind speed exceeds 8 m/s.As the angle of low-speed wind increases,the rotor thrust changes little,the duct thrust increases,and the total thrust increases.In addition,we figure out that cases with the same crosswind ratio are similar in results,and increasing the rotating speed or fan radius is beneficial to performance improvement in wind.The findings are essential to the ducted fan design and UAV flight control design for stable and safe operations in wind conditions.展开更多
Ducted fans are widely used in various applications of Unmanned Aerial Vehicles(UAVs)due to the high efficiency,low noise and high safety.The unsteady characteristics of ducted fans flying near the ground are signific...Ducted fans are widely used in various applications of Unmanned Aerial Vehicles(UAVs)due to the high efficiency,low noise and high safety.The unsteady characteristics of ducted fans flying near the ground are significant,which may bring stability problems.In this paper,the sliding mesh technology is applied and the Unsteady Reynolds Averaged Navier-Stokes(URANS)method is adopted to evaluate the influence of ground on the aerodynamic performance of ducted fans.The time-averaged results show that the ground leads to the decrease of duct thrust,the increase of rotor thrust and the decrease of total thrust.The transient results show that there exist small-scale stall cells with circumferential movements in ground effect.The stall cells start to appear at the blade root when the height is 0.8 rotor radius distance,and arise at both the blade root and tip when the height drops to 0.2.It is found that the unsteady cells rotate between blade passages with an approximate relative speed of 30%-80%of the fan speed,and lead to thrust fluctuations up to 37%of the total thrust.The results are essential to the flight control design of the ducted fan flying vehicle,to ensure its stability in ground effect.展开更多
文摘Because the mover and stator of a doubly-fed linear motor are both equipped with three-phase windings, the motor enables contactless energy to be transferred from the stator to the mover. Thus, when a doubly-fed linear motor is used in the linear driving system of trains, neither an overhead line nor a third rail is needed. However, the doubly- fed motor will lead to more severe thrust fluctuation than the unilateral motors. In order to overcome this shortcoming, the thrust fluctuation of the doubly-fed motor should be analyzed. In this paper, an expression for motor thrust is derived. It points out that the slot effect caused by the slotted structure is the main reason for the increase of thrust fluctuation. The method of adopting unequal pole pitch and unequal slot numbers per pole per phase of stator and mover, is proposed to weaken the slot effect when designing the motor slot parameters. Three different motor models are simulated by ANSOFT. The proposed method results in a motor thrust fluctuation coefficient of 8.4%, compared to 49.4% for the conventional method. Therefore, the motor's thrust fluctuation is effectively suppressed by the proposed method.
基金The National Natural Science Foundation of China(Grant No.51979226).
文摘The requirement of low radiated noise is increasing for underwater propulsors as the noise significantly affecting the comfort and quietness of ships,submarines,and vessels.To broaden the view of noise characteristics of pump-jet propulsors(PJPs),this paper considers the radiated noise of a pre-swirl stator PJP with the effects of the advance coefficient and rotor rotational speed.Radiated noise is obtained by the“hybrid method”approach,which combines a hydrodynamic solver with a hydroacoustic solver.The turbulence flow is obtained through improved delayed detached eddy simulation(IDDES),which show good agreement with the experiment,including the performance and flow field.The solver precision,permeable surface size,and sampling frequency notably affect the noise calculation.The spectra of thrust fluctuation and radiated noise are characterized by the tonal phenomenon around the blade passing frequency and its harmonics.The spectrum of radiated noise and overall sound pressure level(OSPL)are considerably affected by both the advance coefficient and the rotor rotational speed.Overall,the numerical results and analysis given in this paper should be partly helpful in deepening the understanding of the radiated noise characteristics of PJPs.
基金supported in part by the National Natural Science Foundation of China under Grant 51507813。
文摘For a new type of toroidal permanent magnet linear motor(TPMLSM), this paper analyzes the thrust fluctuation in the constant acceleration operation of the motor from the Angle of the cogging force of the linear motor. For the motor whose structure has been determined and processed, the structural parameters of the motor cannot be changed, and its performance cannot be improved from the perspective of the motor body.Therefore, this paper tries to consider the influence of the cogging force on the normal operation of the motor from the perspective of control. In this paper, starting from the body structure of motor, first on the annular linear motor of the cogging force characteristics were extracted, and its expression is obtained by Fourier decomposition, then investigated considering the cogging force and does not consider the cogging force control of motor model, it can be seen that the control performance deteriorates significantly after considering cogging force of the motor, and the acceleration fluctuation increases significantly during the operation of the motor. On this basis, disturbance observation algorithm is introduced, and feedforward compensation is carried out by extracting the characteristic values of the disturbance model. The results show that the disturbance observer can suppress the thrust fluctuation caused by the motor cogging force to a large extent, and it can reduce the peak-to-peak value of the thrust fluctuation by more than 85% during the motor acceleration operation.
基金This study was co-supported by the National Key Research and Development Program of China(No.2020YFC1512500),The Advanced Aviation Power Innovation institution,The Aero Engine Academy of China,and Tsinghua University Initiative Scientific Research Program,China.
文摘Ducted fans have been extensively used in Unmanned Aerial Vehicles(UAVs)for a variety of missions because of high efficiency,high safety and low noise.Wind,as a kind of typical meteorological condition,brings significant aerodynamic interference to the ducted fan,which seriously threatens flight stability and safety.In this work,the numerical simulation with the Unsteady Reynolds Averaged Navier-Stokes(URANS)method and the sliding mesh technique is performed to evaluate the steady wind effect.The results show that the wind will lead to serious unsteady effects in the flow field,and the thrust fluctuates at the blade passing frequency of 200 Hz.As the wind speed increases,the rotor thrust increases,the duct thrust decreases,and the total thrust changes little.Flow instability may occur when the wind speed exceeds 8 m/s.As the angle of low-speed wind increases,the rotor thrust changes little,the duct thrust increases,and the total thrust increases.In addition,we figure out that cases with the same crosswind ratio are similar in results,and increasing the rotating speed or fan radius is beneficial to performance improvement in wind.The findings are essential to the ducted fan design and UAV flight control design for stable and safe operations in wind conditions.
基金co-supported by the National Key Research and Development Program of China(No.2020YFC1512500)The Advanced Aviation Power Innovation institution,The Aero Engine Academy of ChinaTsinghua University Initiative Scientific Research Program.
文摘Ducted fans are widely used in various applications of Unmanned Aerial Vehicles(UAVs)due to the high efficiency,low noise and high safety.The unsteady characteristics of ducted fans flying near the ground are significant,which may bring stability problems.In this paper,the sliding mesh technology is applied and the Unsteady Reynolds Averaged Navier-Stokes(URANS)method is adopted to evaluate the influence of ground on the aerodynamic performance of ducted fans.The time-averaged results show that the ground leads to the decrease of duct thrust,the increase of rotor thrust and the decrease of total thrust.The transient results show that there exist small-scale stall cells with circumferential movements in ground effect.The stall cells start to appear at the blade root when the height is 0.8 rotor radius distance,and arise at both the blade root and tip when the height drops to 0.2.It is found that the unsteady cells rotate between blade passages with an approximate relative speed of 30%-80%of the fan speed,and lead to thrust fluctuations up to 37%of the total thrust.The results are essential to the flight control design of the ducted fan flying vehicle,to ensure its stability in ground effect.