The combined submerged biofilm ( SBF)-activated sludge (AS) process for treatment of municipal wastewater in a small city in China is described in this paper. The process exhibited high removal efficiencies for ca...The combined submerged biofilm ( SBF)-activated sludge (AS) process for treatment of municipal wastewater in a small city in China is described in this paper. The process exhibited high removal efficiencies for carbonaceous substances, nitrogen and phosphorus which mainly took place in the combined SBF-AS biore- actor. The SBF-AS bioreactor was divided into pre-anoxic, anaerobic, anoxic and aerobic zones from inlet to outlet, in which fixed biofilm carriers were packed. Excellent performance had been obtained under normal operating conditions in more than one year of operation in Dong' e municipal WWTP, Shandong province, with mean removal efficiencies of BOD5 93.4%, COD 88%, SS 92%, NH4 - N 82. 1%, TP 75% and TN 66.7%, and quite high effluent quality such as BOD5 6 to 10 rag/L, COD 20 to 40 rag/L, SS 5 to 10 rag/L, TN 10 to 20 rag/L, NH4 - N 4 to 8 mg/L and TP 0. 6 to 1.0 mg/L. The effluent was reused multi-purposely, such as toilet flushing, green belt watering and artificial lake pounding. Simultaneous nitrification and denitrification took place due to the DO gradient in biofilm in aerobic zone of the SBF-AS bioreactor, which made TN removal efficiency improved remarkably in system. Some activated sludge was returned from final clarifiers to the bioreactor for phosphorus removal. The process had the advantages of low investment and low operational/ maintenance (O/M) costs, low sludge yield and was preferably employed in small towns and cities.展开更多
文摘The combined submerged biofilm ( SBF)-activated sludge (AS) process for treatment of municipal wastewater in a small city in China is described in this paper. The process exhibited high removal efficiencies for carbonaceous substances, nitrogen and phosphorus which mainly took place in the combined SBF-AS biore- actor. The SBF-AS bioreactor was divided into pre-anoxic, anaerobic, anoxic and aerobic zones from inlet to outlet, in which fixed biofilm carriers were packed. Excellent performance had been obtained under normal operating conditions in more than one year of operation in Dong' e municipal WWTP, Shandong province, with mean removal efficiencies of BOD5 93.4%, COD 88%, SS 92%, NH4 - N 82. 1%, TP 75% and TN 66.7%, and quite high effluent quality such as BOD5 6 to 10 rag/L, COD 20 to 40 rag/L, SS 5 to 10 rag/L, TN 10 to 20 rag/L, NH4 - N 4 to 8 mg/L and TP 0. 6 to 1.0 mg/L. The effluent was reused multi-purposely, such as toilet flushing, green belt watering and artificial lake pounding. Simultaneous nitrification and denitrification took place due to the DO gradient in biofilm in aerobic zone of the SBF-AS bioreactor, which made TN removal efficiency improved remarkably in system. Some activated sludge was returned from final clarifiers to the bioreactor for phosphorus removal. The process had the advantages of low investment and low operational/ maintenance (O/M) costs, low sludge yield and was preferably employed in small towns and cities.
文摘研究了水力停留时间(HRT)对复合式生物膜-活性污泥工艺处理城市污水效能和反应器中微生物性质的影响.研究结果表明,HRT对系统COD的去除效果影响不大,对氮源污染的影响较大.随着HRT的减少,系统中的污泥质量浓度呈现不断增加的趋势,系统的COD容积去除负荷显著增强.对微生物呼吸速率(OUR)的分析表明,维持较长的HRT能够使反应器内微生物具有更强的活性.因此,建议复合式生物膜-活性污泥工艺合理的HRT的范围为6~8 h.