An experimental study on lost foam casting of an Al-Si-Cu alloy was conducted. The main objective was to study the effect of pattern coating thickness on casting imperfection and porosity percentage as well as eutecti...An experimental study on lost foam casting of an Al-Si-Cu alloy was conducted. The main objective was to study the effect of pattern coating thickness on casting imperfection and porosity percentage as well as eutectic silicon spacing of the alloy. The results showed that increasing slurry viscosity and flask dipping time influenced the casting integrity and microstructural characteristics. It was found that thinner pattern coating produced improved mould filling, refined microstructure and higher quality castings containing less porosity.展开更多
The conventional foaming agents have the problems of poor adaptability and high cost during the application in different types of gas fields,especially in high temperature,high salinity,high acidic gas and high conden...The conventional foaming agents have the problems of poor adaptability and high cost during the application in different types of gas fields,especially in high temperature,high salinity,high acidic gas and high condensate oil and gas fields.In this study,the Gemini foaming agent was used as the main agent to enhance foaming and foam stability of the foaming agent,the grafted nanoparticles were used as foam stabilizer to further improve the foam stability,and the characteristic auxiliaries were added to make the foaming agent suitable for different types of gas reservoirs.Two types and six subtypes of nanoparticle foaming agents have been prepared for the main gas fields of China.The experimental evaluation results show that the overall temperature resistance,salinity resistance,H2S resistance,CO2 resistance and condensate resistance of the nanoparticle foaming agents can reach 160℃,250000 mg/L,100 mg/L,100%and 40%,respectively.The new foaming agents have been used in 8685 wells in China.Compared with conventional foaming agent,the average gas flow rate per well increased by 62.48%,the pressure difference(casing-tubing)decreased by 18.9%,and the cost dropped by 45%.The effect of reducing cost and increasing efficiency is obvious.展开更多
基金Ministry of Science and Technology of Malaysia for funding the research project under E-science Fund Vote No. 79352
文摘An experimental study on lost foam casting of an Al-Si-Cu alloy was conducted. The main objective was to study the effect of pattern coating thickness on casting imperfection and porosity percentage as well as eutectic silicon spacing of the alloy. The results showed that increasing slurry viscosity and flask dipping time influenced the casting integrity and microstructural characteristics. It was found that thinner pattern coating produced improved mould filling, refined microstructure and higher quality castings containing less porosity.
基金Supported by the PetroChina Scientifc Research and Technological Development Project(kt2017-21-14-1).
文摘The conventional foaming agents have the problems of poor adaptability and high cost during the application in different types of gas fields,especially in high temperature,high salinity,high acidic gas and high condensate oil and gas fields.In this study,the Gemini foaming agent was used as the main agent to enhance foaming and foam stability of the foaming agent,the grafted nanoparticles were used as foam stabilizer to further improve the foam stability,and the characteristic auxiliaries were added to make the foaming agent suitable for different types of gas reservoirs.Two types and six subtypes of nanoparticle foaming agents have been prepared for the main gas fields of China.The experimental evaluation results show that the overall temperature resistance,salinity resistance,H2S resistance,CO2 resistance and condensate resistance of the nanoparticle foaming agents can reach 160℃,250000 mg/L,100 mg/L,100%and 40%,respectively.The new foaming agents have been used in 8685 wells in China.Compared with conventional foaming agent,the average gas flow rate per well increased by 62.48%,the pressure difference(casing-tubing)decreased by 18.9%,and the cost dropped by 45%.The effect of reducing cost and increasing efficiency is obvious.