Industrial-scale experiments were conducted to study the effects of tertiary air declination angle(TDA)on the coal combustion and steam temperature characteristics in the first 350-MW supercritical down-fired boiler i...Industrial-scale experiments were conducted to study the effects of tertiary air declination angle(TDA)on the coal combustion and steam temperature characteristics in the first 350-MW supercritical down-fired boiler in China with the multiple-injection and multiple-staging combustion(MIMSC)technology at medium and high loads.The experimental results indicated that as the TDA increased from 0°to 15°,the overall gas temperature in the lower furnace rose and the symmetry of temperature field was enhanced.The ignition distance of the fuel-rich coal/air flow decreased.In near-burner region,the concentration of O2 decreased while the concentrations of CO and NO increased.The concentration of NO decreased in near-tertiary-air region.The carbon in fly ash decreased significantly from 8.40%to 6.45%at a load of 260 MW.At a TDA of 15°,the ignition distances were the shortest(2.07 m and 1.73 m)at a load of 210 MW and 260 MW,respectively.The main and reheat steam temperatures were the highest(557.2℃ and 559.4℃ at a load of 210 MW,558.4℃ and 560.3℃ at a load of 260 MW).The carbon in fly ash was the lowest(4.83%)at a load of 210 MW.On changing the TDA from 15°to 25°,the flame kernel was found to move downward and the main and reheat steam temperatures dropped obviously.The change of TDA has little effect on NO_(x) emissions(660–681 mg/m^(3) at 6%O_(2)).In comprehensive consideration of the pulverized coal combustion characteristics and the unit economic performance,an optimal TDA of 15°is recommended.展开更多
Since the first batch of 350-MW supercritical utility boilers was put into operation, the exhaust flue gas temperature of the boilers has always been higher than the designed value. The main reason is that the heat ab...Since the first batch of 350-MW supercritical utility boilers was put into operation, the exhaust flue gas temperature of the boilers has always been higher than the designed value. The main reason is that the heat absorbed by the air heater is not sufficient. In Huaneng Dongfang Power Plant, the exhaust flue gas temperature is lowered through modifications to the economizer and the air heater. The experimental results reveal that every year, each boiler could save 3 850 tons of standard coal and reduce 85 tons of SO2 and 9 000 tons of CO2 respectively after retrofit.展开更多
This article reviews the problems of Russia-made 800-MW coal-fired supercritical boilers in Suizhong Power Plant, such as burner bumout, water-wall leakage, slag screenⅠexplosion, crack happened on the desuperheater ...This article reviews the problems of Russia-made 800-MW coal-fired supercritical boilers in Suizhong Power Plant, such as burner bumout, water-wall leakage, slag screenⅠexplosion, crack happened on the desuperheater outlet of reheater and welding defect of economizer; tells the process of renovating these units by modifying the original design and adjusting the operation parameters. After several years' effort, all the problems have been well solved. The experience may be useful for other imported units in China.展开更多
The supercritical circulating fluidized bed(CFB)boiler,which combines the advantages of CFB combustion with low cost emission control and supercritical steam cycle with high efficiency of coal energy,is believed to be...The supercritical circulating fluidized bed(CFB)boiler,which combines the advantages of CFB combustion with low cost emission control and supercritical steam cycle with high efficiency of coal energy,is believed to be the future of CFB combustion technology.It is also of greatest importance for low rank coal utilization in China.Different from the supercritical pulverized coal boiler that has been developed more than 50 years,the supercritical CFB boiler is still a new one which requires further investigation.Without any precedentor engineering reference,Chinese researchers have con ducted fundamental research,development,design of the supercritical CFB boilers independently.The design theory and key technology for supercritical CFB boiler were proposed.Key components and novel structures were invented.The first 600 MWe supercritical CFB boiler and its auxiliaries were successfully developed and demonstrated in Baima Power Plant,Shenhua Group as well as the simulator,control technology,installation technology,commissioning technology,system integration and operation technology.Compared with the 460 MWe supercritical CFB in Poland,developed in the same period and the only other supercritical one of commercial running in the word beside Baima,the 600 MWe one in Baima has a better performance.Besides,supercritical CFB boilers of 350 MWe have been developed and widely commercialized in China.In this paper,the updated progress of 660 MWe ultra-supercritical CFB boilers under development is introduced.展开更多
基金This work was supported by the National Natural Science Foundation of China(Grant No.51706054)the China Postdoctoral Science Foundation(Grant No.2019M660633).
文摘Industrial-scale experiments were conducted to study the effects of tertiary air declination angle(TDA)on the coal combustion and steam temperature characteristics in the first 350-MW supercritical down-fired boiler in China with the multiple-injection and multiple-staging combustion(MIMSC)technology at medium and high loads.The experimental results indicated that as the TDA increased from 0°to 15°,the overall gas temperature in the lower furnace rose and the symmetry of temperature field was enhanced.The ignition distance of the fuel-rich coal/air flow decreased.In near-burner region,the concentration of O2 decreased while the concentrations of CO and NO increased.The concentration of NO decreased in near-tertiary-air region.The carbon in fly ash decreased significantly from 8.40%to 6.45%at a load of 260 MW.At a TDA of 15°,the ignition distances were the shortest(2.07 m and 1.73 m)at a load of 210 MW and 260 MW,respectively.The main and reheat steam temperatures were the highest(557.2℃ and 559.4℃ at a load of 210 MW,558.4℃ and 560.3℃ at a load of 260 MW).The carbon in fly ash was the lowest(4.83%)at a load of 210 MW.On changing the TDA from 15°to 25°,the flame kernel was found to move downward and the main and reheat steam temperatures dropped obviously.The change of TDA has little effect on NO_(x) emissions(660–681 mg/m^(3) at 6%O_(2)).In comprehensive consideration of the pulverized coal combustion characteristics and the unit economic performance,an optimal TDA of 15°is recommended.
文摘Since the first batch of 350-MW supercritical utility boilers was put into operation, the exhaust flue gas temperature of the boilers has always been higher than the designed value. The main reason is that the heat absorbed by the air heater is not sufficient. In Huaneng Dongfang Power Plant, the exhaust flue gas temperature is lowered through modifications to the economizer and the air heater. The experimental results reveal that every year, each boiler could save 3 850 tons of standard coal and reduce 85 tons of SO2 and 9 000 tons of CO2 respectively after retrofit.
文摘This article reviews the problems of Russia-made 800-MW coal-fired supercritical boilers in Suizhong Power Plant, such as burner bumout, water-wall leakage, slag screenⅠexplosion, crack happened on the desuperheater outlet of reheater and welding defect of economizer; tells the process of renovating these units by modifying the original design and adjusting the operation parameters. After several years' effort, all the problems have been well solved. The experience may be useful for other imported units in China.
文摘The supercritical circulating fluidized bed(CFB)boiler,which combines the advantages of CFB combustion with low cost emission control and supercritical steam cycle with high efficiency of coal energy,is believed to be the future of CFB combustion technology.It is also of greatest importance for low rank coal utilization in China.Different from the supercritical pulverized coal boiler that has been developed more than 50 years,the supercritical CFB boiler is still a new one which requires further investigation.Without any precedentor engineering reference,Chinese researchers have con ducted fundamental research,development,design of the supercritical CFB boilers independently.The design theory and key technology for supercritical CFB boiler were proposed.Key components and novel structures were invented.The first 600 MWe supercritical CFB boiler and its auxiliaries were successfully developed and demonstrated in Baima Power Plant,Shenhua Group as well as the simulator,control technology,installation technology,commissioning technology,system integration and operation technology.Compared with the 460 MWe supercritical CFB in Poland,developed in the same period and the only other supercritical one of commercial running in the word beside Baima,the 600 MWe one in Baima has a better performance.Besides,supercritical CFB boilers of 350 MWe have been developed and widely commercialized in China.In this paper,the updated progress of 660 MWe ultra-supercritical CFB boilers under development is introduced.