A space-dispersed double-wall jet combustion system was developed by adopting the wall-guiding spray method and the stratification theory.The experimental test was carried out to optimize the structural parameters of ...A space-dispersed double-wall jet combustion system was developed by adopting the wall-guiding spray method and the stratification theory.The experimental test was carried out to optimize the structural parameters of the diesel-engine combustion system,including chamber structure,swirl ratio of cylinder head,included angle of jet orifice,number and diameter of jet orifice,fuel injection pressure and timing.The effect of double-wall jet combustion system on combustion and engine performance was tested to obtain the best performance indexes,and the double-wall jet combustion system was compared to the prototype.The results show that NOx is reduced from 712 PPm to 487 PPm at 2 100 r/min,and from 593 PPm to 369 PPm at 3 000 r/min,which are reduced by 31.6% and 37.7%,respectively.The smoke intensity was reduced form 3.67 BSU to 2.1 BSU,and the oil consumption was reduced from 240.5 g/(kW·h) to 225.4 g/(kW·h),which was decreased by 6.3% at low speed.The pressure in the cylinder was obviously reduced from 115 bar to 108 bar,which was reduced by 6%.展开更多
文摘A space-dispersed double-wall jet combustion system was developed by adopting the wall-guiding spray method and the stratification theory.The experimental test was carried out to optimize the structural parameters of the diesel-engine combustion system,including chamber structure,swirl ratio of cylinder head,included angle of jet orifice,number and diameter of jet orifice,fuel injection pressure and timing.The effect of double-wall jet combustion system on combustion and engine performance was tested to obtain the best performance indexes,and the double-wall jet combustion system was compared to the prototype.The results show that NOx is reduced from 712 PPm to 487 PPm at 2 100 r/min,and from 593 PPm to 369 PPm at 3 000 r/min,which are reduced by 31.6% and 37.7%,respectively.The smoke intensity was reduced form 3.67 BSU to 2.1 BSU,and the oil consumption was reduced from 240.5 g/(kW·h) to 225.4 g/(kW·h),which was decreased by 6.3% at low speed.The pressure in the cylinder was obviously reduced from 115 bar to 108 bar,which was reduced by 6%.