A scramjet combustor with double cavitybased flameholders was experimentally studied in a directconnected test bed with the inflow conditions of M = 2.64,Pt = 1.84 MPa,Tt = 1 300 K.Successful ignition and selfsustaine...A scramjet combustor with double cavitybased flameholders was experimentally studied in a directconnected test bed with the inflow conditions of M = 2.64,Pt = 1.84 MPa,Tt = 1 300 K.Successful ignition and selfsustained combustion with room temperature kerosene was achieved using pilot hydrogen,and kerosene was vertically injected into the combustor through 4×φ 0.5 mm holes mounted on the wall.For different equivalence ratios and different injection schemes with both tandem cavities and parallel cavities,flow fields were obtained and compared using a high speed camera and a Schlieren system.Results revealed that the combustor inside the flow field was greatly influenced by the cavity installation scheme,cavities in tandem easily to form a single side flame distribution,and cavities in parallel are more likely to form a joint flame,forming a choked combustion mode.The supersonic combustion flame was a kind of diffusion flame and there were two kinds of combustion modes.In the unchoked combustion mode,both subsonic and supersonic combustion regions existed.While in the choked mode,the combustion region was fully subsonic with strong shock propagating upstream.Results also showed that there was a balance point between the boundary separation and shock enhanced combustion,depending on the intensity of heat release.展开更多
The flame quenching process in combustors was observed by high speed camera and Schlieren system, at the inflow conditions of Ma = 2.64, To = 1483K, P0 = 1.65 MPa, T = 724 K and P -- 76.3 kPa. Changing process of the ...The flame quenching process in combustors was observed by high speed camera and Schlieren system, at the inflow conditions of Ma = 2.64, To = 1483K, P0 = 1.65 MPa, T = 724 K and P -- 76.3 kPa. Changing process of the flame and shock structure in the combustor was clearly observed. The results revealed that the precom- bustion shock disappeared accompanied with the process in which the flame was blown out and withdrawed from the mainflow into the cavity and vanished after a short while. The time of quenching process was extended by the cavity flame holder, and the ability of flame holding was enhanced by arranging more cavities in the downstream as well. The flame was blown from the upstream to the downstream, so the flame in the downstream of the cavity was quenched out later than that in the upstream.展开更多
文摘A scramjet combustor with double cavitybased flameholders was experimentally studied in a directconnected test bed with the inflow conditions of M = 2.64,Pt = 1.84 MPa,Tt = 1 300 K.Successful ignition and selfsustained combustion with room temperature kerosene was achieved using pilot hydrogen,and kerosene was vertically injected into the combustor through 4×φ 0.5 mm holes mounted on the wall.For different equivalence ratios and different injection schemes with both tandem cavities and parallel cavities,flow fields were obtained and compared using a high speed camera and a Schlieren system.Results revealed that the combustor inside the flow field was greatly influenced by the cavity installation scheme,cavities in tandem easily to form a single side flame distribution,and cavities in parallel are more likely to form a joint flame,forming a choked combustion mode.The supersonic combustion flame was a kind of diffusion flame and there were two kinds of combustion modes.In the unchoked combustion mode,both subsonic and supersonic combustion regions existed.While in the choked mode,the combustion region was fully subsonic with strong shock propagating upstream.Results also showed that there was a balance point between the boundary separation and shock enhanced combustion,depending on the intensity of heat release.
基金supported by the National Natural Science Foundation of China (10902124)
文摘The flame quenching process in combustors was observed by high speed camera and Schlieren system, at the inflow conditions of Ma = 2.64, To = 1483K, P0 = 1.65 MPa, T = 724 K and P -- 76.3 kPa. Changing process of the flame and shock structure in the combustor was clearly observed. The results revealed that the precom- bustion shock disappeared accompanied with the process in which the flame was blown out and withdrawed from the mainflow into the cavity and vanished after a short while. The time of quenching process was extended by the cavity flame holder, and the ability of flame holding was enhanced by arranging more cavities in the downstream as well. The flame was blown from the upstream to the downstream, so the flame in the downstream of the cavity was quenched out later than that in the upstream.