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Summary of Steam System Optimization and Energy Saving and Carbon Reduction Practice in Yanshan Petrochemical Company
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作者 Jianxin GAO 《Asian Agricultural Research》 2022年第8期39-43,共5页
This paper analyzes the main problems of Sinopec Beijing Yanshan Petrochemical Co.,Ltd.,such as decentralized steam system layout,many types of fuels,obvious increase in fuel cost,low operation efficiency of turbine a... This paper analyzes the main problems of Sinopec Beijing Yanshan Petrochemical Co.,Ltd.,such as decentralized steam system layout,many types of fuels,obvious increase in fuel cost,low operation efficiency of turbine and boiler and high self consumption loss,and puts forward and implements optimization and improvement measures such as pressure raising transformation of natural gas system,adjustment of energy consumption structure,reduction of energy consumption cost,improvement of steam production quality and equipment efficiency.The results showed that compared with the fuel consumption in 2018,the consumption of coal coke was reduced by 550000 t,the consumption of natural gas was increased by 170000 t,and the total consumption of fuel gas and fuel oil was increased by 50000 t,equivalent to 246000 t of standard coal;the purchased electricity was increased by about 5×10^(8) kW·h.Green power trading and 14.76 MW distributed photovoltaic projects were carried out.According to the calculation of 1400-1600 h annual power generation in class II photovoltaic areas and the emission factor of North China regional power grid baseline,the annual emission reduction was about 55000 t CO_(2) in 2021.After the above transformation,the goal of zero-coking is achieved;the steam consumption of units is reduced by 21.5%,the steam production of boilers is reduced by 24.9%,and the annual emission reduction is about 760000 t CO_(2),which has achieved good results. 展开更多
关键词 Steam system Fuel structure Energy structure Equipment efficiency Steam loss OPTIMIZATION Energy saving Carbon reduction
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Commercial Application of the MIP-CGP Technology for Olefin Reduction in FCC Unit 被引量:1
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作者 Su Wensheng 《China Petroleum Processing & Petrochemical Technology》 SCIE CAS 2009年第1期25-30,共6页
The refinery of Yanshan Petrochemical Company has twice retrofitted a 2.0-Mt/a RFCC unit with the MIP-CGP technology aimed at maximization of isoparaffins/clean gasoline and increased output of propylene. By modifying... The refinery of Yanshan Petrochemical Company has twice retrofitted a 2.0-Mt/a RFCC unit with the MIP-CGP technology aimed at maximization of isoparaffins/clean gasoline and increased output of propylene. By modifying the riser reactor with addition of the second reaction zone coupled with an added external catalyst cooler outside the regenerator and adoption of the CGP catalyst to control the cracking depth the refiners have realized the target of reducing olefin content in gasoline and increasing the yield of LPG. The results of retrofitting the RFCC unit have revealed that after revamp of FCC unit the yield of LPG was increased by 7.31%, the conversion rate was increased by 9.06%, and the total liquid yield was decreased by 0.3%. After revamp of the RFCC unit the olefin content in gasoline was reduced by 19.5 v%, and the RON rating of gasoline was increased by 0.7 units to meet the demand of Beijing municipality for manufacture of the Olympic clean gasoline. 展开更多
关键词 重油催化裂化装置 CGP 商业应用 蛋白 技术 降烯烃 液化石油气 清洁汽油
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